Power Plant Downsizing Disaster and the Left Behinds
Favorites Post #80
Originally posted December 27, 2014
The Power Plant Men and Women knew that a major downsizing was going to occur throughout the company on Friday, July 29, 1994. The upper management had already experienced the preliminary stages of this particular downsizing since it started at the top. Over a four month period that started with an early retirement, it worked its way down the ranks until the actual Power Plant Men at the plant in North Central Oklahoma were going to be downsized on that one day.
The people that had taken the early retirement (which was available for anyone 50 years and older) had already left a couple of months earlier. Since the downsizing was being decided from the top down, we soon learned that our Plant Manager Ron Kilman would no longer be a Plant Manager. He was too young to take the early retirement. I believe he was 47 at the time.
The person taking Ron’s place was Bill Green, a guy that was old enough to take the early retirement, but decided to stay. Bill was 53 years old at the time. Perhaps he knew in advance that he had a secure position before the deadline to choose the early retirement.
The final week when the downsizing was going to take place, several things were happening that made the entire week seem surreal (this is a word that means — sort of weird and unnatural). I was spending the week in the old Brown and Root building because we were busy training everyone at the plant about Confined Space Safety and the OSHA regulations that we had to follow.
We had to have all the OSHA training completed by August 1 in order to avoid the fines that OSHA had given us back in April (See the post: “Power Plant Men Summoned by Department of Labor“). We had formed a confined space rescue team and taken the required Confined Space training (see the post “Finding and Defining Power Plant Confined Spaces“). We were using the old training room in the old Brown and Root Building because we wanted it to be away from the plant area where the foremen wouldn’t be bothered while they were taking their class.
The first day of training, Ben Brandt the assistant plant manager was in the the class. He was going to be a plant manager at another plant, I think it was the plant in Seminole county.

Seminole Power Plant at night outside of Konawa Oklahoma. This picture was found at: http://www.redbubble.com/people/harrietrn/works/1425122-seminole-power-plant
I could tell that Ben was not interested in being in the training, and given all that was going down that week, I could see why. We would say something in the class about how you had to fill out your confined space permit and turn it in to the Control Room, and Ben would shake his head in disagreement as if he didn’t think that was ever going to happen…. Well, times were changing in more ways than one that week.
Tuesday afternoon was when things really began to get weird…. We knew that Friday would be the last day for a bunch of Power Plant Men, but we didn’t yet know who. During the previous downsizing in 1987 and 1988, we at least knew who was going to leave months before they actually had to leave. Now we were down to just a few days and we still didn’t know who had a job come August 1 (next Monday).
On Tuesday afternoon, one at a time, someone would be paged on the Gaitronics Gray Phone (the plant PA system) by one of the four foremen that had survived.
We were cutting the number of first line foremen in Maintenance from 13 down to 4 and getting completely rid of two levels of management. So, that we would no longer have an A foremen and a Supervisor over each group. So, we wouldn’t have a position like an Electric Supervisor or a Mechanical Maintenance Supervisor.
Our new foremen were Andy Tubbs,
Alan Kramer,
Charles Patten
and Mark Fielder.

Mark Fielder (actually, Mike Vogle was the foreman. Mark Fielder changed roles with him some time after the Re-org)
All great guys!
So, when one of them would page someone on the Gray Phone, we knew that they were going to be asked to meet them upstairs in the main office somewhere. Then they were told that they had a position on that person’s team.
So, picture this scenario. About 160 of the original 218 employees were waiting to learn their fate that week (the rest had retired). It was late Tuesday afternoon when Alan Hetherington told us that they had already begun calling operators to the office to tell them they had jobs. They were not calling anyone to tell them that they didn’t have a job. So, when you heard someone’s name being called, then you knew they were safe (well…. safe is a relative term).
On Wednesday just before lunch, I was called to the office by Alan Kramer. He told me he was going to be my new foreman. I hadn’t really worried about it up to that point, because, well, I just figured that I was pretty well irreplaceable since there really wasn’t anyone else that would go climbing around inside the precipitators during overhauls, so they would want to keep me around for that reason alone.
With that said, it was at least a little less stressful to actually have been told that I did have a position. After all, I had caused so much trouble the previous few years (see 50% of the posts I have written to find out how), enough for some people to hold grudges against me. So, I did have this small doubt in the back of my head that worried about that.
Alan Kramer explained to me that we would no longer have teams for each area of expertise. We wouldn’t have teams of electricians or Instrument and Controls, or Testing, etc. We would be cross-functional teams. We would learn more about that next Monday.
When I returned to the Brown and Root building, the rest of the confined space team asked me if I had a job. I told them I did. At this point, all work at the plant seemed to have ceased. Everyone was waiting around to receive a call on the Gray Phone.
At first, we thought this was going to be like the first downsizing where each person was called to the office and told if they had a job or they didn’t have a job. By Wednesday afternoon, it became apparent that things weren’t working out that way. The only people being called to the office were people that were being told they did have a job. No one was being told if they didn’t.
Either this was a cruel joke being played on the Power Plant Men and Women, or the management hadn’t really thought about the consequences of doing this. It became apparent right away to everyone including those that had been told they had a position that this was a terrible way to notify people about their future. What about those that hadn’t been called to the front office? What were they supposed to think?
About half of the Power Plant Men had received the call, when it seemed that the calls had just stopped some time on Thursday morning. We had finished our last training session in the Brown and Root building and we were just meeting as a team to discuss our next steps in creating Confined Space rescue plans. We were not making much progress, as everyone was just sitting around in a mild state of shock staring into space.
Alan Hetherington had not been called, so he figured that he wouldn’t have a job after Friday. We discussed other people that were being left out. No one on Gerald Ferguson’s team at the coal yard had been called (which included Alan). We later heard that Gerald Ferguson, all distraught that his team had been wiped out was in disbelief that they had let his entire team go. He blamed it on the fact that his team had refused to participate in the Quality Process since it was deemed “voluntary”.
By Thursday afternoon, the stress became so bad for some that they had gone to Jim Arnold and asked him point blank if they had a job after Friday and he refused to say anything to them. Preston Jenkins became so stressed out that he had to go home early because he was too sick with stress.
We knew that Bill Green was the new plant manager.
Jim Arnold was the new Supervisor of Operations and Jasper Christensen was the Supervisor of Maintenance. It seemed to us as if the downsizing was being orchestrated by Jim Arnold, as he was the one going all over the plant on Thursday and Friday coordinating things.
When we came into the office on Friday morning, all the radios had been taken from the electric shop office. I was asked to go up to the logic room and shutdown the Gray phone system. It became clear that Jim Arnold didn’t want anyone listening to what was going on throughout the day.
It was normal having Highway Patrol at the plant, because they were the regular plant guards at the front gate, but today there were a lot of them, and they were in uniform. They were escorting people off of the plant grounds one at a time. We were told that we were not supposed to interact with people being escorted off of the plant grounds. We weren’t supposed to approach them to even say goodbye.
It took the entire day to escort people out of the plant this way. It was very dehumanizing that great Power Plant Men who we had all worked alongside for years were suddenly being treated as if they were criminals and were being escorted off of the plant grounds by armed Highway Patrolmen.
It was just as devastating for those that were left behind. This was a clear indication that those people treating our friends this way were going to be our new supervisors (not our immediate foremen) and that they had a warped sense of superiority. They may have justified their actions in their minds in order to sleep at night, but the reality was that at least one person involved in this extraction of humanity was relishing in his new found power.
No one had been more left behind than the plant manager, Ron Kilman who was too young to accept the retirement package.
He knew he didn’t have a future with the company for the past couple of months as this entire saga had been unfolding at the plant. During the early retirement party for those that were leaving before the slaughter took place, Ron (an avid airplane pilot) had worn a shirt that said, “Will Fly for Food”, which he revealed by opening his outer shirt while introducing some of the retirees. This had brought an applause that was reminiscent of the first day he had arrived some seven years earlier when he told a joke during his first meeting with the plant.
There were those at the plant that had reason to dislike Ron for specific decisions that he had made during his tenure at the plant. One that comes to mind (that I haven’t already written about) is when Ray Eberle’s house was on fire and he left the plant to go fight the fire and make sure his family was safe. Ron docked his pay for the time he was not on the plant grounds since he wasn’t a member of the voluntary fire department. Ron has admitted since that time that there were certain decisions he made while he was Plant Manager that he would have changed if he could.
I felt as if I understood Ron, and knew that he was a good person that wanted to do the right thing. I also knew there were times when a Plant Manager had to make unpopular decisions. I also knew from my own experience that Ron, like everyone else was just as much human as the rest of us, and would occasionally make a decision he would later regret. The times when Ron tried docking my pay after working long overtime hours, I just worked around it by taking vacation to keep my overtime and figured that he was playing the role of Plant Manager and following the rules the way he saw fit.
Some time shortly after lunch, Ron came into the electric shop office and sat down. This was the first time in those seven years that he had come just for a visit and it was on his last day working for the company. Ron just didn’t know what to do.
He explained that no one had told him anything. No one had officially told him to leave. No one had escorted him off of the plant grounds. He wasn’t sure how he was supposed to make his exit. Was he just supposed to go to his car and drive out the gate and never return? No one told him anything.
The way Ron Kilman was treated Friday, July 29, 1994, was a clear representation of the type of people that were left in charge next Monday morning on August 1. The entire plant knew this in their heart. As much grief that was felt by the people being escorted out of the gate after years of loyal service to their company, those that were left behind felt every bit of that grief.
This was the darkest day in the history of the Power plant in North Central Oklahoma. The Power Plant Men left behind by this experience were negatively effected for years after that day. There was a bitterness and sorrow that took a long time to recover in their hearts.
The worst part of the event was that it was so unnecessary. We understood that we had to downsize. We had accepted that some of us would be leaving. Each person at our plant had a level of decency that would accept the fact that when the time came for them to leave, they would hug their friends, say goodbye and with the help of each other, the rest would help them carry their stuff to their car and say goodbye.
We were all robbed of this opportunity. Everyone, even those left behind, were suddenly treated as if we were criminals. We had a “Black Friday” at the plant before, on February 15, 1985 (see the post “Power Plant Snitch“). This time the impact was ten times worse.
All I can say to those who made the decision to handle the layoff this way is: “Shame on you! What would your Mother think if she knew what you did?”
Comment from original post
Power Plant Men Summoned by Department of Labor
Favorites Post #72
Originally posted August 30, 2014.
When a death or a near death occurs at a workplace due to an accident, OSHA (Occupational Safety and Health Administration) will investigate what happened. There are two reasons for this. If they find that the company has been negligent in following the safety regulations set down in CFR 1910, then they are fined (if the negligence is severe enough). OSHA also investigates the accident to see if changes are needed to regulations in order to protect employees due to new unsafe workplace conditions that are not currently covered under CFR 1910.
Because of the tragedy that happened at our plant that I outlined in the post: “Tragedy Occurs During Power Plant Safety Meeting” and after I had met with the OSHA man (Gerald Young) to give him my deposition as discussed in the post last week: “The OSHA Man Cometh“, the plant manager, the assistant plant manager, and I were summoned to the Department of Labor building in Oklahoma City at 10 o’clock on Monday April 18, 1994.
On a side note:
The Department of Labor office in Oklahoma City is just a couple of blocks from the Murrah Federal Building that was bombed exactly one year and one day after our visit on April 19, 1995. Not that there was any connection.
I mentioned this because I went to the Murrah building later that day after the meeting with OSHA to meet my brother for lunch. He was working there in the Marine Recruiting office at the time. I think he was a Major then. He changed jobs in June 1994 and moved to Washington D.C.. His replacement was killed in the bombing. Here he is Greg today as a full Marine Colonel:
End of Side Note:
I was asked by Ron Kilman our plant manager to show up at 9:00 am on Monday in the building south of our main corporate headquarters where we rented office space to meet with the guys from our own Safety Department because they were required to attend the OSHA meeting with us. The Department of Labor building was just across the parking lot and across the street from this building, so we planned to walk from there.
I drove myself because Ron said he had other meetings to attend in Oklahoma City after this meeting was over and he wouldn’t be driving back to the plant. That was why I arranged to have lunch with my brother. I figured that word had gone out from Tom Gibson that I talk a lot during long trips, and he just wanted some peace and quiet that morning.
When we met with the Corporate Safety Department Jack Cox told us how we should act during the meeting with OSHA. He didn’t tell us to do anything wrong, like withhold information. He just told us to answer all the questions as truthfully as we could. Don’t offer any information that isn’t directly asked by OSHA. Don’t argue with them if you disagree.
From what I understood from the conversation, we were supposed to be polite, truthful and don’t waste their time going down a rat hole with specifics. I was told that I shouldn’t have to say anything and I should be quiet unless I was asked a specific question. The Safety department would answer all the questions and make any statements that need to be made. I was assured by them that I had nothing to be worried about. I only needed to tell the truth if asked anything.
If you know my personality, I always want to throw in my 2 cents, even when I know it is wasted on the audience. But I took this seriously. We were going to be fined by OSHA for 10 different violations relating to the accident that occurred at the plant. I was there because I was directly in charge of the work that was being done when the accident occurred. It was my deposition that was used to determine about half of the violations.
After we had been briefed on how we should behave during the meeting, as a group we walked from the corporate building over to the Department Of Labor building. One of the safety guys was carrying a few binders. I think one was the company’s Policies and Procedures book (We called it the GP&P).
Upon entering the building we went to the 3rd floor where we were asked to wait in a room until OSHA was ready for the meeting. The room had a long table down the middle. As usual, I picked a seat about halfway down on one side. I remember Ron Kilman sitting across from me and about 2 seats down.
We waited and we waited….. 10:00 came and went, and no one came. We quietly discussed whether this was to make us more nervous by keeping us waiting. Then someone came to the door and apologized. They said that Robert B. Reich, the U.S. Secretary of Labor was in the office that day and that had thrown off everyone’s schedule.
This was quite a coincidence, and we wondered if Robert B. Reich (it seems like you need to put the B in his name in order to say it right) would be attending our meeting. That would sort of throw a whole new importance of me keeping my mouth shut to make sure I wasn’t putting my foot in it.
It seemed as if Mr. Reich had shown up unexpectedly. Or at least on short notice. Almost as if it was a surprise visit to check up on the place. He didn’t end up coming to our meeting. Now that I think about it. This was one day shy of being one year to the date that the Branch Davidians had burned themselves alive in Waco, which was one year and one day before the Murrah Building Bombing three blocks away from where we were sitting that morning. Aren’t coincidences interesting? Just saying…
More about why Robert B. Reich was there further below.
Around 10:30 four or five OSHA lawyers (I assume they were lawyers, they talked like they were), came in the room along with the Jerry that had interviewed me a few weeks earlier. They apologized again for being late due to the arrival of their “supreme” boss. They sort of sat at one end of the room and the people from our company was more on the other end. Jerry, the OSHA man, sat next to me in the middle.
I was saying a mantra to myself…. “Don’t say anything… just keep quiet and listen…. don’t say anything… just keep quiet and listen.
The meeting began by the Lady at the end of the table reading off the violations to us. I don’t remember all 10. I remember the most important violations. They mainly centered around the new Confined Space section of 1910. It was 1910.146 that dealt with confined spaces and it had gone into affect April 1, 1993, almost one year before the accident happened. Generally, OSHA gives companies about a year to comply to the new regulations, which kind of put us right on the edge since the accident at our plant had occurred on March 3, 1994.
Because of this, some of the violations were quickly removed. That lowered the number down to 6 violations right away. That was good. No one from our company had said a word yet, and already the OSHA lawyers seemed to be on our side. Then they read off a violation that said that our company had not implemented the required Confined Space Program as outlined in CFR 1910.146.
This was when our Safety Department leader, Jack Cox. said that we would like to contest that violation, because here is the company policy manual that shows that we implemented the Confined Space Program before the end of the year.
One of the OSHA lawyers responded by saying that we had not fully implemented it because we had not trained the employees how to follow the policy. When he made that statement, Ron Kilman contested it.
He had a stack of papers that showed that each of the employees at the plant had taken the training and had signed a paper saying they had read the policy. Not only that, but the person that was hurt was not a company employee, they were an outside vendor who was hired by the company to vacuum out the hoppers.
The OSHA man said that just because they took the course did not mean that they were properly trained. Ron asked how do you know they weren’t properly trained. The OSHA man replied, “Because they didn’t follow all the rules. If they had, no one would have been hurt.” — What do you say to that? You can tell we weren’t properly trained because someone was hurt? I suppose that the OSHA rules were written in such a way that if you followed them to the letter, no matter what kind of mechanical failure happens, no one will be hurt. I could see the frustration on Ron’s face.
I was a little amused by Ron’s statement though because Jack Cox had told us to just let them answer all the questions and the first seemingly absurd thing the OSHA man had said, Ron had addressed. — I smiled and said to myself…. “Don’t say anything… just keep quiet and listen…”
One of the violations was that we didn’t have a Confined Space Rescue Team. That was true, we didn’t. There was something in the regulations that said, if a rescue team could arrive in a reasonable time from somewhere else, we didn’t have to have our own rescue team…. Well, we lived 20 miles from the nearest fire station equipped with a Confined Space Rescue team. So, there was that…. That was a legitimate violation.
The next violation was that we didn’t have a rescue plan for every confined space in the plant and each confined space was not clearly marked with a Confined Space sign. This was a legitimate violation.
The next violation was that we hadn’t coordinated efforts between different work groups working in confined spaces together. This was clearly stated in the regulations…. — Oh oh. that was me… I think I was mid-mantra when I heard that one. I had just said to myself… “…anything….just keep….” when I heard this violation. I stopped muttering to myself and immediately forgot that I was supposed to keep quiet.
I said, “But wait a minute. We did coordinate between the three groups that were working in the confined spaces. I was coordinating that. I had posted a sheet on a beam in the middle of the hopper area where the accident occurred where the Brown and Root contractors, and the vacuum truck contractors knew what hoppers were still full and which were safe to enter.
I kept the sheet updated each day and so did the vacuum truck workers. They indicated when they had finished vacuuming out a hopper, and I would inspect it from above. When I deemed it safe, the Brown and Root contractors could enter the space. The accident occurred because one of the vacuum truck workers entered the confined space while still cleaning it out and before I had inspected it to make sure it was safe.”
Jerry (the OSHA man that had interviewed me turned and said, “Oh. I didn’t know that. Do you still have that piece of paper?” — Incredibly, I did. About a week after all the vacuuming had finished and all the hoppers were safe, I was walking through the hopper area under the precipitator where I found the paper with the duct tape still on it laying on the grating. Without realizing the importance, I picked it up and brought it back to the janitor closet behind the electric shop that we now used as a “Precipitator Fly Ash Cleanup Room”. I had laid it on a shelf there. The lawyers said, “Send us the original sheet and we will drop this violation.
Here is a copy of the piece of paper. The big black splotch at the top is what duct tape looks like when you make a copy of it.
Well, that worked out good. I had stepped out of line by opening my mouth before I had been asked a question, but everything worked out all right.
The final verdict was that we had four violations. We had to re-train our employees on Confined Spaces. We had to create a Confined Space Rescue Team. We had to put the correct signs on all of the confined spaces and we had to develop rescue plans for all of the confined spaces on the plant grounds. If we did that by August 1, 1994, the four remaining violations which amounted to a $40,000 fine would all be dropped. So, we had our work cut out for us. This not only impacted our plant, but all the Power Plants. The meeting was adjourned.
I already told you what I did after the meeting (I went and ate lunch with my brother). But I haven’t mentioned yet why Robert B. Reich had made a surprise visit to the Department of Labor building in Oklahoma City on April 18.
As it turned out, that morning, Labor Secretary Reich had come to Oklahoma City to hand deliver a $7.5 million fine to Dayton Tire Company. This was due to an accident that had resulted in a man, Bob L. Jullian, being crushed by a piece of machinery in the tire plant. He died a week and a half later at the age of 53.
Robert B. Reich had become so angry when he had studied the case on Friday that he wanted to hand deliver the citation himself the following Monday. That is how we ended up in the building at the same time on Monday, April 18, 1994. We resolved our dispute with OSHA on a congenial note and the citations were dropped on August 1. Dayton, however, was still fighting the conviction 18 years later, eventually paying around a $2 million penalty.
Now you know the rest of the story. Well, almost. Like I said, we had a lot of work to do in the next three and a half months.
Printing Impossible Power Plant Fast News Post
Favorites Post #54
Originally posted: July 12, 2014:
Tom Gibson, the Electric Supervisor at the Coal-fired Power Plant in North Central Oklahoma didn’t have a clue the large can of worms he opened the day in 1988 when he told me to find out all I could about the company computer in Corporate Headquarters…. The one that ran all the important financial systems for the company. I remember going straight down to the Electric Shop office and sending a request for a username on the Honeywell Mainframe to the IT department, with Tom’s approval.
This story is a continuation of two previous stories…. Last week I wrote a post called: “Power Plant Customer Service Team Gone Wild“. This is the next shoe that dropped in that story…. Earlier this year I wrote a post called: “Toby O’Brien and Doing the Impossible“. Well, this is the second story in the list of “Impossible Things” Power Plant Electricians were able to accomplish when others said it couldn’t be done.
As a reminder… and in case you didn’t read last week’s post…. as a summary….. let me just say that I had printed out a form on every printer in the company as part of a “Quality Idea” our team was investigating. In doing so, I sent commands to the printers to change their quality settings, as well as the Font Size and a few other settings. When I ran the little known command that sent the document to every printer listed on the mainframe, I didn’t realize that this included all the billing, paycheck and work order printers that all had their special kinds of paper and setting for those particular jobs to run.
This was probably the biggest “Faux Pas” (pronounced “Foe Paw” — yeah…. French… which literally means: “False Step”) of my 18 years as an Electrician. Before I tell you about how the second shoe dropped… Let me explain that a few weeks before I had hit enter on the keyboard sending the disastrous command to the Mainframe, In June, 1993, I had found an interesting program on the Honeywell mainframe called “Magna 8”.
It had to do with creating reports from the main database. This was the entire database that ran the Electric Company Business! I thought this would be a great program to learn in order to create all kinds of reports for our plant that would help us understand where our efforts were being spent. I thought I might actually be able to tie our Maintenance Orders to the time the employees spent on them to their wages, and to the cost of the parts used…. Nothing like that existed at the time, and the little I was able to read from the Magna 8 User Manual on the mainframe, this seemed like just the ticket..
We had never heard of SAP, or other ERP systems at the time. — Oh… sorry… ERP stands for “Enterprise Resource Planning”. It does just that. It combines all the company’s business together in one application so that you can account for all the costs down to each machine, person, and part. If I could learn more about Magna 8, maybe I could start piecing these pieces together from the database. I was having one problem…. When I would page down in the user manual, it kept skipping the bottom half of every page….
I couldn’t figure out how to stop it from scrolling past the second half of each page. So, I called in a favor from the IT guys downtown and asked them if they could send me a printed copy of the Magna 8 User’s Manual. They said they would be glad to send me a copy. About a week later, I received the User Manual through company mail. It was about 4 inches thick.
There were different sections. One was called: “The Update Module”. Yeah…. That’s right…. It was used to enter data into the database…. I thought about that module for about 2 seconds and decided It would be best to stay away from that one. Then there was the “Reporting Module”.
That was the one I was looking for. — on a side note…. I know “for” is a preposition, and I know you aren’t supposed to end a sentence in a preposition, however, who doesn’t say, “That’s what I was looking for”? In these circumstances, I figure that I better approach it from a whole different angle…. like…. “That’s the section I really wanted.” — End side note.
A couple of weeks after I received the copy of the Magna 8 User Guide, I sent the infamous form to all the printers in the company, and that’s when I was sort of had all my “atta boys” taken away with that one “Uh Oh”. I was all prepared to watch my step while on the mainframe. About a week after the episode in Tom’s office when he told me not to send anything outside the plant without Ron Kilman’s permission, my foreman, Andy Tubbs came in the office and told me that in two days, I was supposed to go to some training in Oklahoma City.
“Oh. Training!” One of my favorite things! I always liked to learn new things. I asked Andy what the training was for (Oh geez… did I really say that? “For” at the end of the sentence again! — how about “I asked Andy what kind of training would I be taking” — yeah…. that’s what I said…). Andy replied, “Something called ‘Magna 8′”.
Oh No! I hadn’t asked for training! I had just asked for the user guide! Now I was scheduled to go to training in Oklahoma City and I knew that no one at the plant had “okay-ed” it. Now what was I supposed to do? I did the only thing I could think of at the time…. I asked Andy where I was supposed to go at Corporate Headquarters for the class.
Since I knew that this class hadn’t been approved by Tom Gibson or even our A Foreman Bill Bennett, I decided that I was going to go on my own dime…. that is, I wasn’t going to expense anything. I would pay for my own mileage and lunch, etc. Hopefully, no one would notice that I was gone that day. — Anyway, I could always fall back on the fact that my own Foreman Andy had told me to go….
So, when the day came, I drove to Oklahoma City and entered Corporate Headquarters dressed in my cleanest steel-toed work boots and my cleanest tee-shirt!

I chose this picture because they look like my boots, only I never wore the toes out so that you could see the steel toes.
When I introduced myself to the instructor, Scott Overmeyer, I told him I was surprised that I had been scheduled for this class. He told me that since I had requested the User Guide that he figured that I should attend this course so that I would know how to use Magna 8 to create reports. — Well, that explained it.
The classroom was short on computers so we had to share one computer between two people. I sat in the back row on the right side if you are facing the instructor. A young lady sat next to me. Her name was something like Laura Burgert. We didn’t introduce ourselves right off the bat. We spent the morning learning about how our database was structured.
Our database was not what is referred to as a “relational database”. I’m not even sure if that term was being used at the time…. anyway, we had what is called a “Hierarchical Database”. The relationships are more like a family tree. If you needed to connect the data, you had to go up the tree to where you could go back down another branch… sort of like if you were into Genealogy and you were looking for your 3rd cousin twice removed. This was all new to me.
Anyway, this isn’t an important part of this story, so don’t strain your brain trying to figure it out.
When noon came around and we were just breaking for lunch, Laura Burgert said to me, “You’re Kevin Breazile! Oh my Gosh! You’re the guy that printed out that form on everyone’s printers!” I replied, “Yeah, that’s me. I sure was in trouble for that one.”
She replied that they had been trying to do something like that for a long time. Then she explained… “I work in the Communication Department and we create the Fast News Bulletins that are sent out to the printers….”
You see… this was what you had to do before e-mail was available…. When there was some news about the company that they wanted to disseminate to all the employees quickly, they would send out a Fast News bulletin to the printers and we would post it on the bulletin board in our area.
She continued to explain….. We have asked IT to give us a list of printers that we should send the Fast News Bulletins, because we know that our list is old and we are sending some to printers that messes up billing jobs and other things…. I said, “Yeah. I know all about those.”
She continued to explain some more…. IT told us there isn’t any way to tell which printers are good printers and which ones we shouldn’t be sending Fast News Bulletins. I replied, “Well…. I know which ones are good and which ones are not. I have all the forms that were sent to me. You can tell right away by the paper they are printed on, and if that’s not enough to give you a hint, just read the ‘colorful’ notes they wrote to me trying to convince me not to print on their printers anymore…”
Laura said it would be a great help if I could send those forms to her. I said I would do it as soon as I was back at the plant.
When I arrived at the plant the next morning, and Andy Tubbs told me that Tom Gibson was upset when he found that I had gone to Oklahoma City for training when Bill Bennett had mentioned it to him the day before. He had been all hot because he hadn’t approved any training and here I was going off on my own to Oklahoma City. I told Andy…. “Well…. You did tell me to go….” (looking sheepishly innocent).
Anyway, after that I gathered up the stack of around 500 forms and carried them up to the mail room where Denise Anson helped me put them in a small box to mail them to Laura Burgert.
A few weeks went by and Laura called me on the phone. She asked me how I had created the header on the forms. You see, I had created a header with the name of the company and part of the name was normally smaller and had one word over the top of another so….. well…… let me just show you…..
Notice the “GAS/AND” in the middle of the name of the company…. — This doesn’t look like anything to you today, because we now have laser printers and Publishers and all sorts of Word Art at our fingertips. But back then, printing this from a mainframe document took some work…. let me explain, just to give you an idea.
First, I had to space all the way out to where the word GAS starts, then I had to turn on the underline and decrease the font size to the size of the small letters and print out the word GAS then I had to turn off the underline and backspace the three characters, change the font back to the large size, then backspace all the way back to the beginning of the line, then print out the word Oklahoma and a space, then change the font back to small and print out the word AND then change the font back to the large size, and continue with the rest of the line. Yeah… I had to send backspace commands to the printer…. I was pretty proud of my header.
You can see by the Memo above that I had been using it for almost a year. The picture above isn’t even using the “Quality” setting on the printer which even made it look a lot sharper.
Anyway, on with the story…… The Fast News Bulletin’s header had a simple design. The “F” in Fast was created using a bunch of F’s. The A using a bunch of A’s. Like this:
Yeah… pretty embarass… um… I mean exciting huh? Laura was looking for a way to add some Quality to the Fast News Bulletin. I told her that I could create large block letters using the graphic commands on the printer I asked her what her printer ID was and I quickly created a Fast News Bulletin for her with a real header: Laura was excited and said that she may be getting back to me soon…. which she did a few weeks later. She asked if I could attend the first meeting of a new Task Force they had created to enhance the Fast News. I said I would be glad to attend, but I would first have to have permission from my Electric Supervisor before I could go (see? I can actually learn something).
She said she would take care of it…. and she did.
Ben Brandt, our Assistant Plant Manager wanted to know why I was being asked to show up to a Corporate Communication Task Force! — “Uh… I don’t know.” I replied. Knowing that everything I did outside the plant grounds was being questioned after my previous “misstep”.
So, one day I showed up at Corporate Headquarters again. Laura Burgert was there to greet me. She told me where to sit along a big long table in a meeting room. I was to sit about halfway down the table, while she sat on one end of the table.
When others came in, the IT person that was on the committee… I believe his name was Mike Russell sat on the far end from Laura. Laura opened the meeting by explaining the reason for the task force and when she finished she said, “For starters we were thinking that instead of using the ugly Fast News header we have been using, we would like to have a header like this…. And she passed a copy of the Fast News Bulletin I had printed out on her printer that day when she called me.
When Mike Russell saw it, he replied, “Our Printers can’t print a header like this.” Laura looked over at me, as if she wanted me to reply to Mike’s remark. So, I said, “This was printed out on the standard IBM network printer.”
Mike replied by saying, “No. Our printers can’t print like this. It’s impossible.” I repeated that this Fast News was printed out on Laura’s IBM printer from the mainframe just like the regular Fast News is printed out. I even told him that I could send him a copy of the header so that he could print it out and see for himself.
He said, “There’s no need to do that. Our printers can’t print this out.” — Though he held a bulletin in his hands that was printed out on our Standard IBM printer.
At the end of the meeting Laura thanked me for coming. She said, “See? This is what we have been dealing with. They probably weren’t going to be able to go anywhere with this.” I just nodded…. I thanked her for inviting me and I returned to the plant 75 miles north.
I guess it didn’t matter too much. A few months later and we were all being introduced to E-Mail, as I had been running telephone cable all over the plant so that we could set up a new NT Server network using Netware 4.0. Which used Novell’s GroupWise for e-mail. Fast News then just showed up in our Inbox.
It’s funny how things work out. What are the odds? I wreak havoc by sending a “rogue” form to printers that should be left alone, only to have those forms become useful to another department after I was “accidentally” enrolled in a training course where I happened to sit next to the one person in the company that could benefit from that printing blunder. Which then led her to look at ways to improve the Fast News Bulletin that she was responsible for creating….
Then the IT department refused to listen, but it didn’t matter anyway because new Technology quickly came along which began the process of weaning us off of the mainframe and onto a new state of the art network that later allowed us to use SAP a real ERP system that made the Magna 8 application that I went to learn in the first place obsolete.
I guess the Fast News Bulletin for the day is that Technology Moves Fast…. If you aren’t on for the ride, then you will be making statements like “That’s Impossible” and having a student in the 8th grade proving you wrong. It reminded me of what my dad always said when I was growing up… “Don’t ever say you can’t. — There’s always a way.”
Comments from the original post:
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Great story! I still applaud your initiative, enthusiasm, and risk-taking tenacity.
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Thanks Ron.
I am still amazed by how many times I am told that something is impossible when I’m already doing it.
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How they ever let you get out of there is incredible, I guess you were just real popular all over the company LOL and proved things were not impossible too many times, what a group of talent at Sooner in one place unreal
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That’s true Dave. It may sound like I was some lone wolf out there doing the impossible, but the truth is that we were surrounded by great Power Plant Men doing the impossible every day.
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Great story! I have been working with IT equipment since the early 80’s. The changes have been amazing, but I will never forget listening to a print job that made a printer sing (literally). The new printers are amazing, but the experts could make those first ones do the strangest things.
The problem with the early computers, as you found out the hard way, is that almost any change involved programming. And since that early equipment was so costly, much of the testing had to be done on production equipment…….
Anyway, it seems your management made the sensible decision to chalk up your mistake as part of the costs of training and testing.
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Couple of things…My wife is an IT person and I sent the link to this to her. She loved it.
The OSHA Man Cometh
Favorites Post #17 (posted in no particular order)
originally post 8/23/2014
I suppose when you are a Plant Manager, the last person you want to see at your Power Plant doorstep is the OSHA Man! That’s exactly what happened on Thursday, March 10, 1994 at the Coal-fired Power Plant in North Central Oklahoma. He was not paying a social call. He was there to conduct an investigation. One in which I was heavily involved.
In my post from last week, “Tragedy Occurs During Power Plant Safety Meeting” I described a near death accident where a contract worker was engulfed in fly ash in a precipitator hopper. The accident was on all channels on the 5 o’clock news in Oklahoma City. The press was there when the Life Flight helicopter arrived at the hospital where they interviewed the flight crew. The OSHA office in the Federal building a few blocks from the Electric Company’s Corporate Headquarters had quickly assigned someone to the case. Armed with all the authority he needed, he began a full investigation of the accident.
The day before Gerald Young, (the OSHA Man) arrived, I had done some investigation myself into the accident. I was trying to figure out exactly what had happened. Why had someone who thought that he had emptied out a hopper so much so that he climbed inside, had suddenly become engulfed in ash? Where did this large volume of ash come from, and why did it decide to suddenly break loose and fill the hopper at the particular moment when James Vickers had decided to climb into the hopper?
Larry Kuennan, the lead engineer had asked me to show him the hopper from the inside of the Precipitator, so he could have an idea of what took place. I told him he needed to put on a fly ash suit and a full face respirator in order to go into the precipitator. After we were all suited up, I took him on a tour of the inside. A sight few people have had the chance to experience. I could write an entire post just about the experience…. Oh…. maybe I already have. See “Moon Walk in a Power Plant Precipitator”
The hopper we needed to investigate was not at the edge, so, we had to squeeze our way around a few beams in order to see the hopper where the accident took place. When we arrived, I explained that when I had first inspected the precipitator, I had found that the ash had piled up five foot above the bottom of the plates because the feeder wasn’t feeding properly.
So, I had figured that when they were vacuuming out the hopper, the ash that was lodged between the plates (that were 9 inches apart) must have still been there when James climbed into the hopper. Something had caused the ash to give way all at once.
Larry and I climbed down between the hoppers where we could see the bottle racks underneath the plates. The bottles are 30 pound cast iron anchors in the shape of the old style milk bottles. They are used to keep the tension on the wires, which are the electrodes that are normally charged with up to 45,000 volts of electricity when the precipitator is online.
When we sat down to look at the four bottle racks, I noticed right away that one rack of bottles was about a foot and a half lower than the rest of the bottle racks. This didn’t make sense to me at first. I couldn’t think of any way that 176 wires and bottles would be lower than the rest of the wires in the hopper. It was a paradox that took a while to soak in.
When we left, Larry Kuennen made a statement I will never forget. He said, “Until now, I thought that Plant Electricians did nothing but twist wires together. I never thought they worked on things like this.” I replied, “We work on anything that has a wire connected to it. That includes almost everything in the plant.” He replied, “Well, I have a new appreciation for Plant Electricians.”
It wasn’t until I returned to the electric shop and heard Scott Hubbard’s recount of the accident (again). Scott and his crew was working on the roof of the precipitator when the accident happened. He said that when the accident happened he heard a loud bang. Sort of like an explosion.
I told him what I had found inside the precipitator. This could only mean one thing…. An electric insulator on the roof of the precipitator that held up the wires on that bottle rack had broken. When that happened, it fell the foot and half causing all the ash that had been lodged between the plates to be immediately jolted loose, engulfing James Vickers who had just climbed in the hopper below.
After lunch, Scott went up on the roof and opened the portal on the tension house that housed the insulator that held up that row of wires. Sure enough. The three foot by 3 inch diameter ceramic insulator had broken. Something that had never happened at the plant up to that point. A tremendous load must have been put on this insulator, or it must have been defective in order to just break. These insulators are designed to hold up to 10,000 pounds of weight. the weight of the bottles and wires altogether weighed about 6,000 pounds add another 1000 pounds for the beam attached to the insulators on the top of the plates. This meant that at least 3,000 pounds of ash was pressing down from the ash above in order for it to just pull apart.
There was only one person that the OSHA man Jerry wanted to speak to when he arrived at the plant (other than to arrange things). That was me. I was the acting foreman in charge of the operations in, on and below the precipitator when the accident happened. I was also just a regular hourly employee, not so “beholden” to the company that I would participate in any kind of “cover-up”.
The first thing OSHA Jerry wanted to see was the inside of the precipitator. So, I procured a respirator for him, and we climbed up to the landing where one enters the precipitator through side doors. The first thing he did when he arrived at the door was take out a measuring tape to measure the height of the door.
I hadn’t thought about it until that moment, but a new set of OSHA regulations had a new set of Confined Space regulations 1910.146 that dealt specifically with confined spaces. It had gone into effect on April 15, 1993. Here we were almost a year later. I had always treated the precipitator as a confined space, so I had always checked the air quality before I entered it.
So, I asked OSHA Jerry why he measured the size of the door. He said, he was checking if the entrance was “restricted” or “limited”. This was the requirement of a Confined space as stated in OSHA regulation 1910.146. I asked him how small does an entrance have to be to be restricted? He said, “Well. That’s not clearly defined. We could enter the precipitator by bending over and stepping in.
That was the first time I thought that maybe the precipitator itself may not really fit into the strict definition of a confined space. The hoppers do for sure, but does the precipitator? Hmm…. I wondered…. I still do come to think of it. The hoppers were definitely confined spaces by definition… “any space with converging walls, such as a hopper…..”
Oh. I forgot to describe OSHA Jerry. He reminded me a little of the guy who was a sidekick in Cheers named Paul Willson:
Actually, he looked so much like him that I thought of him right away.
When we were done inspecting the precipitator, we returned to the front office where we went to Tom Gibson’s (our Electric Supervisor) office. He closed the door and locked it. And he began to interview me by explaining that anything that was said in this room would be held in confidence. He explained that I could speak freely and that the Electric Company could do nothing to me for telling him the truth.
I thought… Ok…. um…. I have always been known for speaking my mind (maybe a little too much), so he wasn’t going to hear anything that I wouldn’t personally tell the Plant Manager, Ron Kilman to his face. Just ask Ron. I’m sure he would agree that I was pretty open about anything that popped into my mind.
He asked me if I had been trained about the OSHA Confined Space regulations. I responded by saying that we had a class on it one day where we went over our new confined space requirements. That consisted of reading the company policy. I knew that I needed to have a hole watch, and I needed to check the air before I went into a confined space.
We checked to make sure there was 20.9% oxygen, that there was less than 10 parts per million Carbon Monoxide, less than 5 parts per million H2S (Hydrogen Sulfide) and that there was less than 5% explosive vapors. OSHA Jack wrote everything down.
Actually, while I was talking, Jerry asked me to pause often because he was writing everything I said word-for-word on a yellow notepad what I was saying.
While we were talking, I asked him a few questions also. I asked Jack how he decided to work for OSHA. Where he had come from (Kansas. Wichita, I think). How long he had been working for OSHA. Did he enjoy his job….. At times, I could get him to digress and tell me a story about his life.
As we continued with our interview over this grave accident that almost resulted in the loss of someone’s life, I was busy making a new friend. By the time he had asked me everything he needed to know, I knew all about how he had grown up in Kansas, and how he had gone from job-to-job until he had ended up in front of me… interviewing me.
When we had finished the interview, he explained to me that this was an official document that contained all the answers to the questions he had asked me. He said that this would be private and that the Electric Company would not be able to ever see what I said unless I wanted them to see it. I asked him if I could show it to them. He said he would give me a copy of it, and I could do whatever I wanted with it. He asked me to sign it. I did.
I took Jerry to the copy machine in the front office where he made copies for me. When he handed them to me, I shook his hand. I told him I enjoyed talking to him. I also told him that I wished him well. I showed him to the elevator, and he left the plant. I made a copy of the papers that I had signed and went directly to the plant manager Ron Kilman’s office and gave him a copy of the document I had signed.
Ron asked me how it went. I told him that it went fine. Here is everything we talked about. I had nothing to hide. It did amaze me that OSHA Jack thought I might want to “spill the beans” about something as if we were treated like peons where the King had total rule. — I guess he didn’t know that Eldon Waugh had retired in 1987.
From there, I went to Bill Bennett’s office. Bill Bennett was our A Foreman. His office was across the hall from Tom Gibson’s office where I had been interviewed for the previous 3 hours. — Yeah. 3 hours. OSHA Jerry didn’t know Shorthand.
Bill asked me how the interview went. I said it went fine. He said that Ron and Ben Brandt had been worried about me because the interview had lasted so long. Bill said he told them, “Don’t worry about Kevin. He probably has this guy wrapped around his little finger. He’s probably using his ‘psychology’ on him”
I always loved Bill with all my heart. He knew me too well. I told Bill that I knew OSHA Jerry’s life story by the time we were done. Bill smiled…. just like this:
I smiled back at Bill. I returned to the Electric Shop to continue with Unit 1 Overhaul. After all. That was my “real” job. I put on my fly ash suit, my full face respirator, and my rubber boots and returned to the innards of the precipitator to continue where I had left off. I had a lot to think about as I scanned the Precipitator plates and wires in the dark with my flashlight safely strapped around my neck.
Comment from the original post
Great story! And good job interviewing OSHA Jack.
When the OSHA (EPA, OFCCP, EEOC, etc.) Man cometh, whatever was scheduled for that day (week, etc.) was suspended and you do whatever he/she wants. Cost to implement changes was not a factor and permanent effects on plant efficiency or employee morale were of little importance either. At 67 (with increasing arthritis) I’m reminded of OSHA’s “help” every time I have to use both hands to start my recip saw (one to pull the trigger and the other to push the “safety” switch), or when I have to re-start my lawnmower every time I empty the grass bag.
Comment from a repost
ESPs are nasty places to have to hang out. We had a guy who was severely burned by flowing ash from a bottom hopper–due to this and some other unrelated health complications which occurred during his absence, he was never able to return to work. For some reason he thought the hopper was empty but it wasn’t and when he opened the door, the ash poured out like water and severely burned his legs. Your story reminded me of the incident. I can’t imagine the impact of being nearly completely engulfed in hot ash. It is a miracle that the man survived.
A Power Plant Halloween Election Story
Originally posted on October 27, 2012:
I can’t say that the Coal-fired Power Plant located in the middle of the North Central Plains of Oklahoma had visitors on Halloween Night trick-or-treating looking for candy. I have mentioned before that we had an evil plant manager when I first arrived as a summer help at the plant that did what he could to make life miserable for his employees. That would sometimes send chills up your spine.
I could tell you stories about the coffin houses on top of the precipitators. I already told you about the Bug Wars in the Basement (see: “Power Plant Spider Wars and Bugs in the Basement“), and even about the Boiler Ghost that ate Bob Lillibridge (See: “Bob Liilibridge Meets the Boiler Ghost“). Instead, I’ll tell a simple story about the Evil Plant Manager and his bees.
One time out of the blue when I was a summer help in 1980, the Plant Manager asked me in a suspiciously benevolent voice if I would stay after work to help him tend to his bees. You see. Eldon Waugh was a beekeeper.
Beekeeping is a noble profession, and I admire their ability to make a good thing out of a seemingly bad situation. Sonny Karcher was a beekeeper. Sonny was a Hero of Mine.
The plant grounds was a great place for bees because we had fields full of clover. But Eldon and bees? I have a slightly different take on it. Bees are industrious workers that are single-minded. They each have their job, and they go about doing it. They are willing to give their life for their hive and in that way, are sort of unsung heroes. Or maybe bees do sing about their heroes and we just don’t know it. Maybe their buzzing away is at times a lament for those who have worked their wings away to the point that they are no longer able to contribute.
Sort of reminds you of a Power Plant Man.
Since I was carpooling at the time and didn’t have my own car, Eldon said that he would drive me back to Stillwater and drop me off at the corner of Washington and Lakeview where I normally was let off, where I would walk up to the University Estates where my parents lived (and still do – or did when I first wrote this post. Now they live across the street from me in Round Rock, Texas). So I went to Eldon’s office when I finished work that day, and I followed him down to his pickup truck. We drove up by the coalyard where he had a trailer that had a bunch of white boxes lined up, which housed his beehives.
Eldon Waugh gave me a hood that beekeepers wear to keep the bees from finding out what the beekeeper really looks like so the bees don’t attack them later when they are flying by and realize that they are the person that keeps interrupting their beehive.
Eldon explained to me that when a bee stings you, you don’t grab the stinger and pull it out because that injects the bee’s venom into your body when you squeeze it. Instead you take a straight edge, like a knife or piece of thin cardboard or something similar and you scrape it off.
That’s when I realized that Eldon had only given me a hood. He hadn’t given me a full beekeeper suit like I would see on TV or in the neighborhood when I was young and some beekeeper came to collect a swarm of bees that had settled in a tree across the street from our house.
Eldon proceeded to open the beehive boxes and inspect them. He had me hold things while he was doing this. He showed me things like how the Queen was kept in a smaller box inside the bigger one that kept it from leaving. Somehow this reminded me of the ball of fire in the boiler that produced the steam that turns the turbine that makes the electricity at the plant.
When he went to open one box he told me that this particular box had bees that were more troublesome than the other bees, and they liked to sting. “Ok.” I thought. “Thanks for letting me know.” Like that was going to help.
I had already resigned myself to the idea of being stung by a bee that was unhappy that the beekeeper had called an unscheduled inspection of the beehive when Eldon jumped back; Pulled off his hood and started batting around in the air. Sure enough. A bee had climbed up under his hood and had stung him on the back of the neck.
I took a key out of my pocket and scraped the stinger off as he whimpered and pointed to where the stinger was jabbing him. The bee was on his collar making peace with his maker (because bees die after they sting you) as I wiped him away. Besides that one incident, the rest of the time went smoothly. Eldon inspected his beehives. It seemed like he was looking for mold or moisture or some such thing. He was satisfied. When we left he gave me a jar of his “Eldon Waugh” Honey that he used to sell at the Farmer’s Market in Stillwater. Then he drove me back to Stillwater.
There was something surreal about this experience, and in a few days, I was compelled to write a poem about it. This is not a poem about Beekeepers in General. This is a poem about Eldon Waugh, the Beekeeper as I saw him. I don’t know where I placed it, so I can’t quote it now, so I’ll remake it up the best I can. You have to excuse me, because I am not a poet (as you could tell with the Bob Lillibridge Meets the Boiler Ghost story), so bear with me. It is short:
The Beekeeper
Bees diligently gathering nectar,
Weaving honey for the hive.
Pouring life into their work,
Spending energy for queen to stay alive.
Beekeeper gives shelter to be safe,
Benevolent ruler over all.
Sharing fields of flowers not of his making,
Protecting helpless and small.
When time to pay the dues,
Beekeeper expects all to comply.
If one tries to deny his share,
Sting him once and you will die.
Why is this a Halloween story? I know I speak harshly of Eldon Waugh and I know that when he went home he had a family like everyone else. I know that Bill Moler his assistant plant manager was the same way. If you met him at Church or somewhere else, he would treat you with the dignity that you deserved. Something happened to them when they drove through the plant gates (I felt), that made them think they were invulnerable and all powerful. Like Mister Burns in the Simpsons (as I was reminded this week).
It was Lord Acton (John Emerich Edward Dalberg Acton) in a letter to Bishop Mandell Creighton in 1887 that said, “Power tends to corrupt, and absolute power corrupts absolutely. Great men are almost always bad men”. At this particular power plant, because it was so far removed from Corporate Headquarters and any other Electric Company departments, the situation allowed the Plant Manager to be an absolute ruler. There wasn’t anyone there to look out for the employees.
A union had come through when the power plant was first coming online trying to get the plant to vote to join the union. Many employees had worked for unions before, and they preferred the tyranny of the evil plant manager over the stifling corruption of the union.
I remember the first summer I was at the plant (in 1979) when everyone was abuzz about the union election. Some people thought it would stop this “absolute power” syndrome infesting the two top dogs. Those employees that had worked for unions warned the rest that to me sounded like joining a union was like selling their soul to the devil. Some had even left their former employers to escape what they referred to as the “manipulation of their morals”. It came down to voting for the lesser of two evils.
I would like to point out that Lord Acton said that Great men are almost “Always” bad. There are exceptions. There was one great liberating moment in Power Plant history at our plant that occurred in 1987 the day that our new plant manager arrived at our plant. His name is Ron Kilman.
Ron called the maintenance department to a meeting to introduce himself to us in the main break room. I remember that when he began speaking he told us a joke about himself. I don’t recall the joke, but I do remember the reaction of the room. I’m sure our reaction puzzled Ron, because we were all stunned.
I gave Charles Foster a look that said, “I didn’t know Plant Managers could joke!” There must be some mistake. No rattling of chains. No “sacrifice your lives and families to provide honey for my table.” Ron was a rather likable person. It didn’t fit. What was he doing as a Plant Manager?
Throughout the almost 7 years that Ron was the plant manager, we were free from the tyranny of the “Beekeeper”. I have invited Ron to read my blog posts because he is one Plant Manger that even though he wasn’t one of the True Power Plant Men in the field showing their character daily by fighting dragons and saving fair maidens, he was our benevolent dictator that had the power to put his thumb down on the rest, but choosing “Might for Right” as King Arthur preferred.
Ok, so Ron Kilman doesn’t look exactly like King Arthur. That would be stretching it a little. Also… I’m sure some people found some reason to not like Ron Kilman through the years that he was Plant Manager. That would be because he made some unpopular decisions from time to time. That is the life of a Plant Manager.
When Ron first came to the plant, he really wanted to stay at the level of the regular working person. I believe that he meant it when he told us that. As the years went by, the demands of managing the large plant occupied so much of his time that little time was left to spend with the people he cared about.
I remember him saying that his manager demanded him to be downtown in Corporate Headquarters so many days a week, and that left him little time at the plant. He asked me what I thought would be a solution to this problem. I told him that I thought he should have a representative that would stay at the plant in his stead that would perform Plant activities and report to him directly. Sort of as an extension of himself. I was not thinking of his Assistant Plant Manager because he had his own job to do.
I was sometimes taken aback when Ron would ask a question like that because it surprised me that he valued my opinion. I will discuss Ron Kilman and why I believe that he is a man of great character in a later post. I only mention him here to show the contrast between Eldon Waugh and Ron. Both were in a position of ultimate power over their employees. One took the high road, and one took the low. Neither of them had ever been to Scotland as far as I know (ok. I had to add another rhyme… geez).
I also titled this post as a “Halloween Election” story. I told you the scary part… that was the story about the beekeeper, in case you forgot to be frightened by it. I also threw in the part about the Union Election as a meager attempt to rid the plant of total managerial tyranny. But the real reason I made this a story about an Election is because of the striking similarity between Ron Kilman and Mitt Romney. My Gosh! Have any of you noticed this? Am I the only one that sees the resemblance? Notice the chin, the hairline and even the gray side burns.
Happy Halloween, and good luck with the next election.
Comment from last Repost:
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Thanks, Kevin. I appreciate your kind words. And thanks for inviting me to receive these posts. I love reading them and remembering my days with the Power Plant Men at Sooner. And by the way, we lived in University Estates too (at 30 Preston Circle).
Making Friends from Foes – A Tale of Power Plant Woes
Originally posted April 25, 2014:
Later in life, thinking back to when I was young, I sometimes wonder at how my first real friend, Mark Schlemper remained my friend throughout my childhood. I remember as a boy, there were times when I wasn’t the friendliest friend. Sometimes I was downright selfish. Mark, on the other hand, was always considerate. Not in an Eddie Haskell way, but in a sincere way. I learned a lot about being a kinder person from Mark, and I’m forever grateful.
I think if Mark had not been my friend during my childhood, then this story would have a very different ending.
Last Friday (April 18, 2014), I posted a story called “Vertan or Sand and Making Enemies of a Power Plant Man“. At the end of that post I explained that I had become the enemy of a team leader during the “We’ve Got The Power” program. I explained this program in the post: “Power Plant ‘We’ve Got The Power’ Program“. With all that said, here is the story:
I was a plant electrician at a coal-fired power plant in North Central Oklahoma when we took part in the “We’ve Got The Power” program. At the time, I was in charge of maintaining the Unit 1 precipitator. The precipitator is what takes the ash out of the exhaust from the boiler, so that you don’t normally see smoke coming out of a Power Plant Smokestack.
My bucket buddy in the Electric Shop, Diana Brien was on a team that tried an experiment on the Unit 1 precipitator by injecting sand into the intake duct in the hope that it would increase the performance. I didn’t put much faith in the experiment, because it was based on something that had happened almost a year earlier when sand was burned in the boiler in order to burn off the oil that had been soaked into the sand.
I hadn’t seen any sand build up in front of the precipitator during the next overhaul, and didn’t believe that any of it had been able to make it’s way through the economizer and the air preheaters to the precipitator.
When Ron Kilman asked me about it, I said that I didn’t think it would do any good, but also, it wouldn’t do any harm either, so I told Ron that I couldn’t see any reason not to do the experiment. Who knows. Maybe something unexpected would happen. — Something did, but not quite in the way anyone would have expected.
On the day of the experiment, sand was blown into the intake duct of the precipitator. When the experiment was taking place, Diana Brien sat at the precipitator computer behind the Unit 1 Alarm Panel in the Control Room. She was printing out readings every so many minutes as the experiment progressed.
At times, I walked by and checked on her to see how it was going. One time when I was standing there watching the readings on the computer, all of the sudden the Opacity shot up. Opacity is used to measure how much smoke is going out of the smoke stack. Something definitely happened to cause a large puff of smoke.
I switched screens to look at the power on each of the control cabinets. After a few seconds I found that cabinet 1A10 had zero Volts on the secondary side of the transformer. It should have been somewhere above 40 Kilovolts. The cabinet hadn’t tripped, but it wasn’t charging up the plates. Cabinet 1A10 was in the very back row of the precipitator, and when the power shuts off on the cabinet it readily lets go of the ash that had built up on it when the rappers on the roof strike the plates.
When I saw the puff occur, I knew where to go look, because this happened whenever one of the back cabinets was turned off. I told Dee that it looked like a fuse had blown on the cabinet. The ash was going to continue billowing out of the precipitator for a couple of hours if I didn’t go do something about it. So, I told Dee that I was going to go to the Precipitator Control Room and replace the fuse.
I passed through the electric shop to grab my tool bucket and headed out to the precipitator. When I arrived, I found the cabinet just as it had indicated on the computer. The fuse had obviously failed. Interesting timing. Coincidence? I thought it was. The fuses controlling the back cabinets were usually the ones that blew because we ran them at a much higher voltage than the rest of the cabinets (at the time).
I quickly replaced the fuse (after attaching grounding cables to the leads, and using a pair of high voltage gloves). Then I powered the cabinet back on.
I returned to the Control Room and told Dee that I replaced the fuse on cabinet 1A10. The opacity had returned to normal. I watched a few more minutes to make sure everything had stabilized, and then I left.
When Ron Kilman was evaluating the results of the experiment, he could plainly see that something strange had happened. Smoke had been pouring out of the smoke stack in the middle of the experiment. So, he asked me what I thought about it.
First of all, as a disclaimer, our team had our own experiments we had been conducting on the precipitator in hopes of coming up with money savings ideas. So, when I told Ron what had happened with the fuse blowing, I wondered if he would trust me to tell the truth, since I had my own skin in the game.
I explained in detail to Ron how the fuse had blown and that I was standing next to Dee watching the computer when the smoke started blowing out of the stack. I could tell that a fuse had blown by looking at the readings, so I went out and replaced the fuse. I told him that fuses do blow periodically in the back of the precipitator, but I couldn’t explain why it happened to fail at that particular time. After I gave him my explanation, he seemed satisfied that I was telling the truth.
I think a token amount of points were awarded to the team because something obviously had happened during the experiment, though it wasn’t clear that sand had anything to do with it. On the other hand, our team was awarded a large amount of points for increasing the precipitator performance using a different method that I may bring up in a later post. To the team that burned the sand, this looked a lot like foul play.
The leader of the team was the Shift Supervisor Jim Padgett. He became very upset when he found out that I had gone to the precipitator control room during the experiment and worked on the equipment. Our team had been awarded a lot of points that was enough to purchase the dining room table set that I have in my dining room today:
It became known throughout the control room and the electric shop that Jim Padgett viewed me as his enemy. The other electricians would jokingly refer to Jim as my “friend”, knowing that Jim had basically declared “war” on me. Any time someone in the shop would have something to say about Jim, they would say, “Kevin’s friend” Jim Padgett….”
When I first became aware that Jim was upset with me, I understood why. If I had been in his shoes I would probably feel the same way. It’s a rotten feeling when you believe that someone has cheated you out of something important. So, I decided up front that I was going to become Jim’s best friend. This is where I think my memory of Mark Schlemper with his patience for me as a boy helped me with this decision.
I had determined that any time Jim asked me to do something I wouldn’t hesitate to help him. It took about a year before Jim could look at me without grimacing. Finally, one day, he asked me if I would go look at something for him to see if we needed a clearance, or if it was something that could be fixed right away. It was something minor, but I knew that this was an indicator that the ice was finally beginning to melt. I was able to fix the problem on the spot, and returned to let him know.
Once we were on semi-speaking terms again, I took an opportunity one day to ask Jim if he would like to join our Computer Club. I had started a Computer Club in the Electric Shop. Anyone could join it for a one time fee of $5.00 that was used to buy shareware and disk cases. For a while I also published a newsletter letting the members of the club know what games and such we had that could be checked out.
Once Jim Padgett joined the Computer Club, it was much easier to have a regular conversation outside of the normal daily business. I had put the thought in my mind when I decided that Jim was going to become my best friend that nothing would make me happier than to be able to do something for Jim. That way, no matter what I was doing at the time, if Jim asked me to do something for him, I would drop whatever I was doing and do my best to help.
I could go on and on explaining how gradually over time, not only was Jim my friend, but Jim acted more and more as if I was his friend as well. Let me just say that the entire process took almost exactly ten years. I can remember the exact moment when Jim indicated to me that I had become his friend.
Here is what happened:
The phone next to my bed rang at 2:15 in the morning on Thursday February 17, 2000. I instantly knew what it meant when the phone rang in the middle of the night. It meant that someone at the plant was calling because there was a problem. Who else would be up on in the middle of the night? The night shift of course.
When I answered the phone, Jim Padgett said, “I hate to wake you up buddy.” I replied, “No. That’s okay. What’s up?” Jim explained that the dumper was down and a train was about halfway through dumping the coal and everything was dead in the water. I said, “Ok. I’ll be right out.”
I turned to Kelly and told her that I had to go fix the dumper. She already knew of course. I pulled on a pair of jeans, a flannel shirt, and on the way out the door, I slipped on my work boots and laced them up. Then I drove the 30 miles out to the plant.
It was just before 3:00 am when I arrived. I grabbed my hardhat from the electric shop and took the elevator up to the Control Room. Jim apologized again and told me that how the dumper acted when it shutdown. I went back down the elevator to the electric shop where I grabbed the key to the pickup truck and my tool bucket and left the electric shop into the cool night air.
Power Plants at night take on magical properties. It’s hard to explain. Lights shining from the 25 story boilers, noises from steam pipes. Hums from motors and transformers. Night Hawks screeching.
When I arrived at the coalyard, I went straight into the Dumper Switchgear where the relays that controlled the dumper were mounted. Having worked on the dumper for the past 17 years, I could troubleshoot the circuits in my sleep. — Actually, I may have done just that. It didn’t take long, and I had replaced a contact on a relay that had broken and had the Coalyard Operator test the dumper long enough to know it was going to work.
When I returned back to Control Room Jim was sitting in the Shift Supervisor’s office. I walked in and showed him the small relay contact that had caused the failure. Jim, looked at me and said something that I thought only a friend would say so casually. I won’t use his exact words, though I remember not only the exact words, I remember his exact expression. He indicated to me that he had passed some gas, and he was apologizing about it. I replied, “Well. That happens.” (No. Not the other thing that happens). I told him I was going to go home. It was about 3:40 by that time.
Jim wished me a good night, and smiling with gratitude, thanked me again for coming out. As I was going back to the parking lot, and on the way home driving through the dark, tired from being woken up in the middle of the night, I had a great feeling of peace. That brief conversation with Jim just before I left was so pleasant in an odd way that I knew we had become friends. This was such a long way from where we had been 10 years earlier when Jim had literally wanted to kill me (well, not that he actually would…).
When I arrived home, I peeled my clothes off in the utility room to keep from tracking coal all over the house. I set the small broken relay contact on the kitchen table as a token to my wife, so she could see why I was called out when she wakes up in the morning. I climbed back into bed around 4:15 to sleep for another two hours.
That morning when I arrived at the plant, the first thing I learned was that about the time that my alarm had woken me up that morning, Jim Padgett had left his shift and driven to his home in Ponca City. When he walked in the door to his house, he collapsed and died instantly of a heart attack. That would have been about 3 hours after the moment that we had said goodbye.
I grieved for Jim’s wife Jane, who had worked for a while at the plant before marrying Jim, but I didn’t grieve for Jim. Something told me, and maybe it was Jim, that he was at peace. In the moment that I heard about Jim’s death, I burned the conversation we had just had that morning into my mind so that I would never forget it.
To this day whenever I know that someone is upset with me for something that I have done to them personally (which still happens occasionally), I am determined that they will become one of my best friends. I will do anything for that person if they ask (unless, of course it is to “not be their friend”). I have my childhood friend Mark Schlemper to thank for the attitude that helped me decide to reach out to Jim Padgett. Without that experience while growing up, Jim and I would never have become friends.
I would like to leave you with a song that reminds me of Jim whenever I hear it. It is called “Bright Eyes” from the movie “Watership Down”. Art Garfunkel sings it:
Note: If you are not able to watch the video above, try clicking this link: Bright Eyes, Art Garfunkel
Comments from the original post:
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I’m glad that you were able to work through a tough situation and reach the point of friendship. although, it does make the loss harder to accept.
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Your story would have been a matter of course for my grandparents and immediately understood and admired by my parents. I suspect that telling it to today’s children might draw blank stares …
Midwestern values likely still include such behaviors, at least for a reasonable number of people. I doubt many folk on the coasts would identify with it. We have lost a lot and have yet to learn the price of that, seems to me.
Turning the Tables on a Power Plant Telephone Interloper
Originally posted June 13, 2014:
When discussing Telephones at the Coal-Fired Power Plant in North Central Oklahoma, I have to remember that some of my readers have a completely different perspective of telephones than me. My children grew up probably never seeing a real rotary dial phone except in movies or old TV shows. It might be a little hard for them to imagine a telephone being a possible murder weapon. Telephones have come a long way since I grew up in the 1960’s and 70’s.
When you turned the dial on a Rotary phone you put your finger in the hole on the number you want to dial and then you swing it around until your finger bumps up against the metal bracket. When you pull your finger out of the hole, the phone sends a rapid succession of pulses to the telephone company telling them what number you just dialed. It was very… well…. tedious and manual…. and not even electronic. It was electric signals and switches. “Mechanical” is the word I think I’m trying to say.
Even the way you received a dial tone was by sending something called a “Ring-to-ground” signal to the telephone company. That would happen when you would lift the receiver off the hook. There are only two wires used to communicate in an old phone and only one of those had voltage on it. when you ground that wire (called the “Ring”) momentarily, the phone company would then send a dial tone to your phone.
You could actually do this on a dead phone line at times when the phone company had shut off your service. On an old pay phone, when the proper coin was inserted in the phone, the coin itself was used to ground the ring wire, thus telling the telephone company to send the dial tone, allowing you to use the phone. In 1983 there was a movie called “Wargames”.
I had learned about how these telephones worked from Bill Rivers just before going to watch this movie. During the movie Matthew Broderick’s character needed to make a phone call at a pay phone but didn’t have a coin. By taking the mouthpiece off of the transmitter, and using a metal pop top he found on the ground, he was able to ground the “ring” wire to the pay phone, and he received a dial tone. There was a good ol’ boy sitting behind me in the movie theater that said, “You can’t do that!” — Being the newly educated smart (-alec) guy I was, I turned around and said, “Yeah. You really can.”
Anyway. This isn’t a story so much about how old phones work. I just wanted to bring the younger readers back-to-date on phones since now they don’t really call them telephones anymore. It is more like, “Smart Phone” and “Cell Phone”, “Mobile Phone” or just “Phone”. The phone in the house isn’t even referred to as a telephone. We now call them “Home Phone” to distinguish them from the actual phones that we use.
Anyway, when I joined the electric shop in 1983, I learned about the phone system. We didn’t use the older Rotary Dial phones at the plant. We were one step up. We had “Touch Tone” Phones.
As I have mentioned in previous posts, we had our own telephone computer at the Power Plant. It was called a ROLM phone system. See the post “A Slap In the Face at a Gas-fired Power Plant“.
To give you an idea of the technology used by this phone system, you connected to it using a “teletype” terminal that you connected to a telephone by clipping the receiver in a cradle. Then you dialed the phone computer. When you connected, it was at 300 Baud. Think of 300 bytes per second, only using audio…. like a fax machine. — It was like connecting using a modem. 300 baud meant that when it typed out the results on the paper that scrolled out the top, you could watch it as it slowly printed out each line. The maximum speed of the terminal was 300 baud.

This is the TI Silent 700 Terminal. We used this exact model of Teletype terminal at the Power Plant
In this picture you can see the cradle in the back where the phone receiver would fit in those two rubber cups.
After many years of going to the lab to connect to the telephone computer to make changes and to monitor the telephone traffic, in 1992 I decided to bring my 8088 computer to work and set it on the desk in the electric shop. We didn’t have our own computer yet. At that time the only people that had computers were office workers and the Shift Supervisor. We had started a computer club and having a computer in the shop was a big help. I had just replaced this computer at home with a 486.

This is a Leading Edge computer. My father had this one. An earlier version than the 8088 that I was using.
I had a modem on my computer, so I tried connecting to the telephone computer, and it worked! So, sometimes during lunch when Charles Foster and I were sitting there talking about movies we had seen while eating vegetables from his garden, I would connect to the ROLM computer and just watch the call log. I could see whenever someone was dialing in and out of the plant.
We had a special call in number into the plant that allowed you to make “trunk” calls. This is another term you don’t hear much anymore. You see….. for the younger readers (again)…. long distant calls used to cost a lot of money. You would be charged by how many minutes you were on the call. During the day, it could be as high as $3.00 a minute to call across the country. Amazing huh? Because today, most of you with cell phones and even your land lines (which are rarely real land lines anymore) long distant phone calls are now free with your phone plan.
Yeah, if you wanted to call someone in the next town over, you would have to pay a fee for every minute you were on the call…. That was when AT&T had a monopoly on the phone lines in the United States. Sure, you only payed $7.00 each month for your phone, but you could only call people in your immediate area or you would be charged extra.
A Trunk line gave you access to a much wider area. The Electric company had a trunk line that gave them access to most of Oklahoma. You could dial into a local number that would connect you to the company phone system. Then after entering the correct password number, you could dial access numbers that would take you to another office location in the electric company. Once on that phone system, you could dial to get an outside line, and then dial a local number in that area.
Our plant had three access numbers that allowed you to dial out locally to Stillwater, Ponca City and Pawnee. This was useful when a foreman needed to call people out to work. They could dial into the plant, then back out to one of these other towns and then dial the local phone number of the crew member they were trying to reach without incurring a personal charge on their phone line.
So, here I was in 1992 during lunch watching the phone traffic in and out of the plant (not exactly NSA style, but sort of), when I saw something unexpected. A long string of numbers showed up. Someone had dialed in on the Stillwater trunk, then dialed out to the Corporate Headquarters trunk, then out to Oklahoma City and from there they placed a long distance call to a phone number in the same area code. The prefix on the phone number was familiar to me. It was a Ponca City phone number. I had lived in Ponca City for three years when I had just been married, from 1986 to 1989. I knew a Ponca City phone number when I saw one.
I thought this was odd, because it wouldn’t be normal for someone to dial from Stillwater through our plant to Oklahoma City only to call a Ponca City phone number when they could have dialed the local Ponca City access code. Then they wouldn’t have had to make a long distance call which bypassed our trunk call system causing the electric company to be billed for the long distance telephone call.
At the time I was a CompuServe user. This was when the World Wide Web was in it’s infancy. I was still using a DOS computer. When I connected to the Internet, it was either by using my dad’s Internet account from Oklahoma State University where I would use Telnet to access a bunch of mainframe computers all over the country, or I would use the DOS-based version of CompuServe. CompuServe was the king of Internet access before America Online came around and seemingly overnight made CompuServe obsolete.
In 1992, CompuServe had a service where you could look up phone numbers and find out whose number it was. Imagine that! Yeah. That was one of the neatest features on CompuServe! That and getting stock quotes. — Like I said…. There was no “www.whitepages.com” online. The only catch to using the reverse phone number feature, was that it was like making a long distance call. It cost money. You were charged by the minute for using the CompuServe reverse telephone number service, with the least amount being a dollar.
So, I bit the bullet and accessed the Phone Number lookup section of CompuServe. I quickly typed in the number. When the name and address of the user popped up, I quickly hit “Print Screen”, and then exited the service. My fee came to $1.00, but at least I knew what number had been dialed in Ponca City.
Charles, Scott Hubbard and I were a little excited by the time Terry Blevins walked into the electric shop office after lunch was over, I told him what I had seen.
When I told Terry the name of the person that had received the long distance call, he recognized the name right away. When I gave him the address, he was sure he knew who it was. The phone number belonged to the Music Director at the Ponca City High School. His son was attending college in Stillwater, Oklahoma.
Well, that sort of cinched it. We had a pretty good idea who had made the call. It was a college student calling home, who had been given the phone number most likely by a fellow student who knew the code to call home in Oklahoma City. So, the only local access code this guy knew was how to dial through our plant to Oklahoma City and back out where he was free (but it was not free for us) to make a long distance call home.
Armed with this knowledge, I headed up to the front office. I went straight to the Plant Manager, Ron Kilman’s office. I told Ron what I had found. I explained in detail how the person had dialed from Stillwater into our plant and then to Oklahoma City and out and then placed a long distance call to Ponca City leaving us with the phone bill. Since it was the middle of the day, the cost of a long distance call was not cheap.
I told Ron that I had used CompuServe to lookup the phone number and that Terry had said that it belonged to the Music Director at the Ponca City High School and that he had a son in college in Stillwater. I was all ready to pounce on this guy. This was a fraudulent use of the telephone service and there were some pretty strict laws then about stealing long distance from someone else.
Ron, being the more level-headed of the two of us thought about it for a minute and said, “What would be the best way to stop this from happening?” — Oh. Well. I was so intent on catching the culprit, I hadn’t thought about that angle…. “Well….” I said, “We could change the pass code used to log into our phone system. We would just have to tell our supervisors what the new number is.”
Ron asked me what it would take to do that. I told him I could do it in two minutes. We quickly settled on a new 4 digit pass code and I left his office and returned to the electric shop and made the change essentially turning the tables on the Telephone Interloper. I suppose the college student in Stillwater was lucky that our plant manager at the time was the type to forgive and forget.
Three years later the entire electric company phone system was replaced by a new AT&T computer which was managed by AT&T. As you can tell… Technology just keeps moving forward making seemingly really neat new inventions quickly obsolete.
Comments from the original post:
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I still stand in awe at all the talent we had at the plant- never has one place had so many guys of remarkable skill and overall just good people and kind hearted.
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I can’t agree with you more! We had the cream of the crop for sure.
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Your memory still amazes me. I don’t remember that at all.
I’ll bet most young people today don’t know why we say to “dial” a phone number!-
It was just a moment in your busy day. It was the highlight of my week.
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Printing Impossible Power Plant Fast News Post
Originally posted: July 12, 2014:
Tom Gibson, the Electric Supervisor at the Coal-fired Power Plant in North Central Oklahoma didn’t have a clue the large can of worms he opened the day in 1988 when he told me to find out all I could about the company computer in Corporate Headquarters…. The one that ran all the important financial systems for the company. I remember going straight down to the Electric Shop office and sending a request for a username on the Honeywell Mainframe to the IT department, with Tom’s approval.
This story is a continuation of two previous stories…. Last week I wrote a post called: “Power Plant Customer Service Team Gone Wild“. This is the next shoe that dropped in that story…. Earlier this year I wrote a post called: “Toby O’Brien and Doing the Impossible“. Well, this is the second story in the list of “Impossible Things” Power Plant Electricians were able to accomplish when others said it couldn’t be done.
As a reminder… and in case you didn’t read last week’s post…. as a summary….. let me just say that I had printed out a form on every printer in the company as part of a “Quality Idea” our team was investigating. In doing so, I sent commands to the printers to change their quality settings, as well as the Font Size and a few other settings. When I ran the little known command that sent the document to every printer listed on the mainframe, I didn’t realize that this included all the billing, paycheck and work order printers that all had their special kinds of paper and setting for those particular jobs to run.
This was probably the biggest “Faux Pas” (pronounced “Foe Paw” — yeah…. French… which literally means: “False Step”) of my 18 years as an Electrician. Before I tell you about how the second shoe dropped… Let me explain that a few weeks before I had hit enter on the keyboard sending the disastrous command to the Mainframe, In June, 1993, I had found an interesting program on the Honeywell mainframe called “Magna 8”.
It had to do with creating reports from the main database. This was the entire database that ran the Electric Company Business! I thought this would be a great program to learn in order to create all kinds of reports for our plant that would help us understand where our efforts were being spent. I thought I might actually be able to tie our Maintenance Orders to the time the employees spent on them to their wages, and to the cost of the parts used…. Nothing like that existed at the time, and the little I was able to read from the Magna 8 User Manual on the mainframe, this seemed like just the ticket..
We had never heard of SAP, or other ERP systems at the time. — Oh… sorry… ERP stands for “Enterprise Resource Planning”. It does just that. It combines all the company’s business together in one application so that you can account for all the costs down to each machine, person, and part. If I could learn more about Magna 8, maybe I could start piecing these pieces together from the database. I was having one problem…. When I would page down in the user manual, it kept skipping the bottom half of every page….
I couldn’t figure out how to stop it from scrolling past the second half of each page. So, I called in a favor from the IT guys downtown and asked them if they could send me a printed copy of the Magna 8 User’s Manual. They said they would be glad to send me a copy. About a week later, I received the User Manual through company mail. It was about 4 inches thick.
There were different sections. One was called: “The Update Module”. Yeah…. That’s right…. It was used to enter data into the database…. I thought about that module for about 2 seconds and decided It would be best to stay away from that one. Then there was the “Reporting Module”.
That was the one I was looking for. — on a side note…. I know “for” is a preposition, and I know you aren’t supposed to end a sentence in a preposition, however, who doesn’t say, “That’s what I was looking for”? In these circumstances, I figure that I better approach it from a whole different angle…. like…. “That’s the section I really wanted.” — End side note.
A couple of weeks after I received the copy of the Magna 8 User Guide, I sent the infamous form to all the printers in the company, and that’s when I was sort of had all my “atta boys” taken away with that one “Uh Oh”. I was all prepared to watch my step while on the mainframe. About a week after the episode in Tom’s office when he told me not to send anything outside the plant without Ron Kilman’s permission, my foreman, Andy Tubbs came in the office and told me that in two days, I was supposed to go to some training in Oklahoma City.
“Oh. Training!” One of my favorite things! I always liked to learn new things. I asked Andy what the training was for (Oh geez… did I really say that? “For” at the end of the sentence again! — how about “I asked Andy what kind of training would I be taking” — yeah…. that’s what I said…). Andy replied, “Something called ‘Magna 8′”.
Oh No! I hadn’t asked for training! I had just asked for the user guide! Now I was scheduled to go to training in Oklahoma City and I knew that no one at the plant had “okay-ed” it. Now what was I supposed to do? I did the only thing I could think of at the time…. I asked Andy where I was supposed to go at Corporate Headquarters for the class.
Since I knew that this class hadn’t been approved by Tom Gibson or even our A Foreman Bill Bennett, I decided that I was going to go on my own dime…. that is, I wasn’t going to expense anything. I would pay for my own mileage and lunch, etc. Hopefully, no one would notice that I was gone that day. — Anyway, I could always fall back on the fact that my own Foreman Andy had told me to go….
So, when the day came, I drove to Oklahoma City and entered Corporate Headquarters dressed in my cleanest steel-toed work boots and my cleanest tee-shirt!

I chose this picture because they look like my boots, only I never wore the toes out so that you could see the steel toes.
When I introduced myself to the instructor, Scott Overmeyer, I told him I was surprised that I had been scheduled for this class. He told me that since I had requested the User Guide that he figured that I should attend this course so that I would know how to use Magna 8 to create reports. — Well, that explained it.
The classroom was short on computers so we had to share one computer between two people. I sat in the back row on the right side if you are facing the instructor. A young lady sat next to me. Her name was something like Laura Burgert. We didn’t introduce ourselves right off the bat. We spent the morning learning about how our database was structured.
Our database was not what is referred to as a “relational database”. I’m not even sure if that term was being used at the time…. anyway, we had what is called a “Hierarchical Database”. The relationships are more like a family tree. If you needed to connect the data, you had to go up the tree to where you could go back down another branch… sort of like if you were into Genealogy and you were looking for your 3rd cousin twice removed. This was all new to me.
Anyway, this isn’t an important part of this story, so don’t strain your brain trying to figure it out.
When noon came around and we were just breaking for lunch, Laura Burgert said to me, “You’re Kevin Breazile! Oh my Gosh! You’re the guy that printed out that form on everyone’s printers!” I replied, “Yeah, that’s me. I sure was in trouble for that one.”
She replied that they had been trying to do something like that for a long time. Then she explained… “I work in the Communication Department and we create the Fast News Bulletins that are sent out to the printers….”
You see… this was what you had to do before e-mail was available…. When there was some news about the company that they wanted to disseminate to all the employees quickly, they would send out a Fast News bulletin to the printers and we would post it on the bulletin board in our area.
She continued to explain….. We have asked IT to give us a list of printers that we should send the Fast News Bulletins, because we know that our list is old and we are sending some to printers that messes up billing jobs and other things…. I said, “Yeah. I know all about those.”
She continued to explain some more…. IT told us there isn’t any way to tell which printers are good printers and which ones we shouldn’t be sending Fast News Bulletins. I replied, “Well…. I know which ones are good and which ones are not. I have all the forms that were sent to me. You can tell right away by the paper they are printed on, and if that’s not enough to give you a hint, just read the ‘colorful’ notes they wrote to me trying to convince me not to print on their printers anymore…”
Laura said it would be a great help if I could send those forms to her. I said I would do it as soon as I was back at the plant.
When I arrived at the plant the next morning, and Andy Tubbs told me that Tom Gibson was upset when he found that I had gone to Oklahoma City for training when Bill Bennett had mentioned it to him the day before. He had been all hot because he hadn’t approved any training and here I was going off on my own to Oklahoma City. I told Andy…. Well…. You did tell me to go….
Anyway, after that I gathered up the stack of around 500 forms and carried them up to the mail room where Denise Anson helped me put them in a small box to mail them to Laura Burgert.
A few weeks went by and Laura called me on the phone. She asked me how I had created the header on the forms. You see, I had created a header with the name of the company and part of the name was normally smaller and had one word over the top of another so….. well…… let me just show you…..
Notice the “GAS/AND” in the middle of the name of the company…. — This doesn’t look like anything to you today, because we now have laser printers and Publishers and all sorts of Word Art at our fingertips. But back then, printing this from a mainframe document took some work…. let me explain, just to give you an idea.
First, I had to space all the way out to where the word GAS starts, then I had to turn on the underline and decrease the font size to the size of the small letters and print out the word GAS then I had to turn off the underline and backspace the three characters, change the font back to the large size, then backspace all the way back to the beginning of the line, then print out the word Oklahoma and a space, then change the font back to small and print out the word AND then change the font back to the large size, and continue with the rest of the line. Yeah… I had to send backspace commands to the printer…. I was pretty proud of my header.
You can see by the Memo above that I had been using it for almost a year. The picture above isn’t even using the “Quality” setting on the printer which even made it look a lot sharper.
Anyway, on with the story…… The Fast News Bulletin’s header had a simple design. The “F” in Fast was created using a bunch of F’s. The A using a bunch of A’s. Like this:
Yeah… pretty embarass… um… I mean exciting huh? Laura was looking for a way to add some Quality to the Fast News Bulletin. I told her that I could create large block letters using the graphic commands on the printer I asked her what her printer ID was and I quickly created a Fast News Bulletin for her with a real header: Laura was excited and said that she may be getting back to me soon…. which she did a few weeks later. She asked if I could attend the first meeting of a new Task Force they had created to enhance the Fast News. I said I would be glad to attend, but I would first have to have permission from my Electric Supervisor before I could go.
She said she would take care of it…. and she did.
Ben Brandt, our Assistant Plant Manager wanted to know why I was being asked to show up to a Corporate Communication Task Force! — “Uh… I don’t know.” I replied. Knowing that everything I did outside the plant grounds was being questioned after my previous “misstep”.
So, one day I showed up at Corporate Headquarters again. Laura Burgert was there to greet me. She told me where to sit along a big long table in a meeting room. I was to sit about halfway down the table, while she sat on one end of the table.
When others came in, the IT person that was on the committee… I believe his name was Mike Russell sat on the far end from Laura. Laura opened the meeting by explaining the reason for the task force and when she finished she said, “For starters we were thinking that instead of using the ugly Fast News header we have been using, we would like to have a header like this…. And she passed a copy of the Fast News Bulletin I had printed out on her printer that day when she called me.
When Mike Russell saw it, he replied, “Our Printers can’t print a header like this.” Laura looked over at me, as if she wanted me to reply to Mike’s remark. So, I said, “This was printed out on the standard IBM network printer.”
Mike replied by saying, “No. Our printers can’t print like this. It’s impossible.” I repeated that this Fast News was printed out on Laura’s IBM printer from the mainframe just like the regular Fast News is printed out. I even told him that I could send him a copy of the header so that he could print it out and see for himself.
He said, “There’s no need to do that. Our printers can’t print this out.” — Though he held a bulletin in his hands that was printed out on our Standard IBM printer.
At the end of the meeting Laura thanked me for coming. She said, “See? This is what we have been dealing with. They probably weren’t going to be able to go anywhere with this.” I just nodded…. I thanked her for inviting me and I returned to the plant 75 miles north.
I guess it didn’t matter too much. A few months later and we were all being introduced to E-Mail, as I had been running telephone cable all over the plant so that we could set up a new NT Server network using Netware 4.0. Which used Novell’s GroupWise for e-mail. Fast News then just showed up in our Inbox.
It’s funny how things work out. What are the odds? I wreak havoc by sending a “rogue” form to printers that should be left alone, only to have those forms become useful to another department after I was “accidentally” enrolled in a training course where I happened to sit next to the one person in the company that could benefit from that printing blunder. Which then led her to look at ways to improve the Fast News Bulletin that she was responsible for creating….
Then the IT department refused to listen, but it didn’t matter anyway because new Technology quickly came along which began the process of weaning us off of the mainframe and onto a new state of the art network that later allowed us to use SAP a real ERP system that made the Magna 8 application that I went to learn in the first place obsolete.
I guess the Fast News Bulletin for the day is that Technology Moves Fast…. If you aren’t on for the ride, then you will be making statements like “That’s Impossible” and having a student in the 8th grade proving you wrong. It reminded me of what my dad always said when I was growing up… “Don’t ever say you can’t. — There’s always a way.”
Comments from the original post:
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Great story! I still applaud your initiative, enthusiasm, and risk-taking tenacity.
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Thanks Ron.
I am still amazed by how many times I am told that something is impossible when I’m already doing it.
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How they ever let you get out of there is incredible, I guess you were just real popular all over the company LOL and proved things were not impossible too many times, what a group of talent at Sooner in one place unreal
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That’s true Dave. It may sound like I was some lone wolf out there doing the impossible, but the truth is that we were surrounded by great Power Plant Men doing the impossible every day.
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Great story! I have been working with IT equipment since the early 80’s. The changes have been amazing, but I will never forget listening to a print job that made a printer sing (literally). The new printers are amazing, but the experts could make those first ones do the strangest things.
The problem with the early computers, as you found out the hard way, is that almost any change involved programming. And since that early equipment was so costly, much of the testing had to be done on production equipment…….
Anyway, it seems your management made the sensible decision to chalk up your mistake as part of the costs of training and testing.
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Couple of things…My wife is an IT person and I sent the link to this to her. She loved it.
I was given a chance to stay with OG&E. Dave Nunez called me at 10:30 one Wednesday night. He said I could have a job in Corporate Headquarters. I asked what the job description was. He said he “didn’t know”. I asked what the salary was. He said he “didn’t know”. I asked about the transition from my current salary to the new salary. He said he “didn’t know”. I asked how long I had to decided about this new job. He said “Before you hang up.” I have NEVER regretted not being a part of that new OG&E gang!