Runaway Fire Hydrant Leaves Power Plant in the Dark
Favorites Post #13 (posted in no particular order)
Originally posted May 17, 2014:
Don’t believe it when the Electric Company tells you that the reason your town lost electricity for an hour was because a squirrel climbed onto a transformer and shorted it out. The real reason just may be more bizarre than that and the company doesn’t want you to know all the different creative ways that power can be shut off. This is a tale of just one of those ways. So, get out your pencil and paper and take notes.
One spring day in 1993 while sitting at the Precipitator computer for Unit one at the Coal-fired Power Plant in North Central Oklahoma, while I was checking the controls to make sure all the cabinets were operating correctly, suddenly there was a distant boom, and the lights in the control room went out. The computer stayed on because it was connected to an electric panel called the VSP or Vital Services Panel, which in turn was supplied by the UPS system (Uninterruptible Power Supply). That was one of those moments where you may pause for a moment to make sure you aren’t still at home dreaming before you fly into a panic.
The Precipitator cabinets all indicated on the computer that they had just shutdown. I rose from the chair and walked around to the front of the Alarm Panel for Unit one, and found that the fluorescent lights were only out on Unit 1. The lights were still on for Unit 2. The Control Panel was lit up like a Christmas Tree with Green, Red, Blue and Yellow Lights. The Alarm Printer was spewing out paper at high speed. As the large sheets of paper were pouring out onto the floor, I watched as Pat Quiring and other brave Power Plant Control Room operators were scurrying back and forth turning switch handles, pushing buttons, and checking pressure gauges.
Just this site alone gave me confidence that everything was going to be all right. These Control Room operators were all well trained for emergencies just like this, and each person knew what their job was. No one was panicking. Everyone was concentrating on the task at hand.
Someone told me that we lost Unit 1, and the Auxiliary Power to Unit 1 at the same time. So, Unit 1 was dead in the water. This meant, no fans, no pumps, no lights, no vending machines, no cold water at the water fountain and most importantly, no hot coffee!!! I could hear steam valves on the T-G floor banging open and the loud sound of steam escaping.
I turned quickly to go to the electric shop to see what I could do there in case I was needed. I bolted out the door and down the six flights of stairs to the Turbine-Generator (T-G) basement. Exiting the stairway, and entering the T-G basement the sound was deafening. I grabbed the earplugs that were dangling around my neck and crammed them into my ears. Steam was pouring out of various pop-off valves. I ducked into the electric shop where across the room Andy Tubbs, one of the electric foreman was pulling large sheets of electric blueprints from the print cabinet and laying them across the work table that doubled as the lunch table.
When I asked Andy what happened, I learned that somehow when a crew was flushing out a fire hydrant the water somehow shot up and into the bus work in the Auxiliary Substation (that supplies backup power to the Power Plant) and it shorted out the 189,000 volt substation directly to ground. When that happened it tripped unit 1 and the auxiliary substation at the same time leaving it without power.
I will explain how a fire hydrant could possibly spray the bus work in a substation in a little while, but first let me tell you what this meant at the moment to not have any power for a Power Plant Boiler and Turbine Generator that has just tripped when it was at full load which was around 515 Megawatts of power at the time.
Normally when a unit trips, the boiler cools down as the large Force Draft (FD) Fans blow air through the boiler while the even larger Induced Draft (ID) fans suck the air from the boiler on the other end and blow the hot air up the smoke stack. This causes the steam in the boiler tubes to condense back into water. Steam valves open on the boiler that allow excessive steam to escape.
When the boiler is running there is a large orange fireball hovering in space in the middle of the boiler. The boiler water is being circulated through the boiler and the Boiler Feed Pump Turbines are pumping steam back and forth between the turbine generator and the boiler reheating the steam until every bit of heat from the boiler that can be safely harnessed is used.
When all this stop suddenly, then it is important that the large fans keep running to cool down the steam, since it is no longer losing energy in the generator as it was when it was busy supplying electricity to 1/2 million people in Oklahoma City. The power is fed to the fans from the Auxiliary substation located right outside the Main Switchgear where all the breakers reside that supply the power to the fans. Unfortunately, in this case, the Auxiliary substation was shutdown as well, leaving the boiler without any fans.
Without fans for cooling, and pumps to circulate the water, the walls of the boiler began heating up to dangerous temperatures. Steam was whistling out of pop off valves, but if the steam drum on the top of the boiler were to run dry, then the entire boiler structure could be compromised and begin melting down. — So, this was serious. Something had to be done right away. It wouldn’t be as bad as the China Syndrome since we were burning coal instead of nuclear power, but it would have caused a lot of damage nonetheless.

From the movie “The China Syndrome” where a similar emergency existed only in the movie, it was a Nuclear Plant
I have a side story about this picture, but I think I’ll save it for another post because I don’t want to digress from the main story at this point (Ok. Let me just say “Jack Maloy and Merl Wright” for those who can’t wait. See the post: “Power Plant Conspiracy Theory“).
With the prospect that the boiler might melt to the ground in a pile of rubble, it would seem that the main priority was to turn the Auxiliary Substation back on so the fans could be turned back on and prevent the boiler from collapsing. So, we walked out to the substation and looked at the switches that would have to be operated in order to first power up the main bus and then to close to supply power to the two big transformers and the six smaller transformers that supplied the Unit 1 Main Switchgear.
While inspecting the switches where the electricity had gone to ground we found that one of the main insulators was cracked.
Since this insulator was cracked, we didn’t really want to operate the switch to test if another 189,000 volts would go straight to ground again, especially since one of us would be standing right underneath it cranking the switch. So, we went back to the shop to find an alternative.
By this time the Plant Manager, Ron Kilman arrived in the shop, and understanding the urgency to find a solution asked us what were the alternatives. He was relying on our expertise to make the decision.
The other solution would be to cut the power over from Unit 2 which was still humming away pushing electricity to Oklahoma City out of the 345,000 volt substation. The cut over would be very simple because the switchgear was designed with this in mind. We analyzed the power rating on the auxiliary transformers on Unit 2 and thought that we might be cutting it close to have them running both sets of fans at the same time, especially since the full load amps of a huge fan starting up was about 10 times the normal rate.
The transformer was rated to handle the load, but consider this. What if this caused Unit 2 to trip as well. With the Auxiliary substation offline, if Unit 2 tripped, we would be in twice the amount of trouble we were currently in. What a day it would have been if that had happened and two 250 foot boilers had come crashing to the ground in a pile of rubble. After reading the power ratings on the auxiliary transformers I was thinking, “Yeah, let’s do it! These transformers can handle it.” Andy was not so eager.
So, we were left with one alternative. That was to shut the switch in the Auxiliary substation that had the cracked insulator and take our chances that it wasn’t going to short to ground and blow up over our heads. I think I was eager to close the switch for Andy, but if I remember correctly, he didn’t want me to be the one to suffer the consequences and decided to close the switch himself. Needless to say. Andy closed the switch, and nothing blew up.
As soon as the power was restored to the switchgear, the fans were powered up and the temperature in the boiler was quickly reduced. The coffee pot in the Electric Shop began heating the coffee again. The power plant was saved from a major catastrophe. That was delayed for another day… of which I will talk about later (see the post “Destruction of a Power Plant God).”
So, how exactly does a fire hydrant shoot water up into the bus work of a substation like the picture of the switch directly above? The culprit fire hydrant wasn’t in the substation, it sat alongside it outside the fence a good 50 feet from the high voltage switch. No hose was attached to the fire hydrant. It was only being flushed out as part of a yearly activity to go around and make sure the fire hydrants are all operating correctly.
Here is the story about how the squirrel climbed into the transformer this time….
George Alley, Dale Mitchell and Mickey Postman were going around to the 30,000 fire hydrants on the plant ground (ok. maybe not that many, but we did have a lot of them), and they were opening up the valves and flushing them out. That means, they were letting them run for a while to clear them out from any contaminates that may have built up over the year of not being used.
Throughout their adventure they had opened a multitude of Hydrants situated out in the fields along the long belt conveyor from the coalyard and around the two one-million gallon #2 Diesel tanks.
The brave Power Plant Men, learned that when opening a fire hydrant wide open in the middle of field had unintended consequences. It tended to wash out the ground in front of the flow of the water shooting out of the hydrant. So the team of experts devised a plan to place a board in front of the hydrant when it would be in danger of tearing a hole in the terrain. The board would divert the water into the air where it would fan out and not cause damage to the surrounding area.
This was working fine, and when they arrived at the fire hydrant next to the substation, since the stream from the hydrant was pointing directly into the substation (hmm. a design flaw, I think), they decided to prop the board up against the fence to keep from washing away the gravel in the substation. Well. When a fire hydrant is opened that hasn’t been used for a year, the first flow of water to shoot out is dark brown.
You may think that this is because the water has somehow become dirty over the past year, but that isn’t quite the case. What has happened is that the pipe has been rusting little by little and the water has become saturated with the rust. So, the water shooting out of the hydrant was full of rust (hence the need to flush them out).
Well. Rust is made of metal. Metal is conductive, especially when it is mixed with water. When the water hit the board, it was deflected into the air and happened to direct itself directly into the high voltage switch in the substation. This caused a circuit to the ground which, once it created an arc pumped all the electricity directly into the ground.
Normally when something like this happens it doesn’t trip the Main Power Transformer to a Power Plant.
This time it did. I know there was a few heads scratching trying to figure it out. I think I figured out what happened a little while later. You see… here is the rest of the story….
Once the unit was back online and the emergency was over, someone finally noticed that the telephone system couldn’t call outside of the plant. Well. I was the main telephone person at the time, so the control room called me and asked me to look into the problem.
I checked the telephone computer and it was up and running just fine. Internal calls could be made. Only any call outside just concluded with a funny humming sound. After checking the circuit in the Logic Room next to the Rolm Telephone Computer I headed for…. guess where….. the Main Switchgear….
In the middle of the main switchgear in the back of the room right next to the Auxiliary Substation beyond the back wall, the outside telephone line came into the plant. The first thing it did was go through a special Telephone Surge Protector.
In this picture above, the silver circular buttons on the left side are really an old style surge protector. whenever there was a power surge, the carbon connection in the surge protector would quickly melt causing the circuit to go straight to ground. Thus protecting the rest of the telephone circuit. So, if some kid in their house decides to connect the 120 volts circuit to the telephone for fun to see what would happen, this circuit would protect the rest of the phone circuits. Keep in mind that this was during the early 1990 when “Surge Protection” still was basically all “mechanical”.
Anyway, when I arrived at this panel and I checked the surge protector to the main line going out of the plant, guess what I found…. Yep. Shorted to ground. Luckily there were some spares that were not wired to anything in the panel and I was able to swap them out for the ones that had been destroyed. — These were a one time use. Which meant, if they ever had to short to ground, they had to be replaced.
Ok. Fine. After a little while, we were able to call back out of the plant, though there was still some residual noise on the line. It was like this… when you called out of the plant, the person on the other end sounded like they were buried in a grave somewhere and they were trying to talk to someone living just like in an episode of the Twilight Episode where a phone line landed on a grave and the dead person tried to call his long lost love from the past.
I didn’t give it much thought other than that I figured the 189,000 volt arc to ground must have shorted out the telephone line since the phone line ran directly under the auxiliary substation ground grid.
It wasn’t until the next morning when the Southwestern Bell repairman showed up at the plant. I knew him well, since he had been working on our phone lines since before the AT&T breakup in 1984. When I met him in the front of the electric shop, he said that he needed to check our telephone circuits. I told him that I knew that we had a problem because we had a high voltage short to ground yesterday and I found our surge protectors melted away.
He explained to me that not only was our circuit affected, but that every relay house from here to Ponca City was blown out. That’s when I realized that the problem was the reverse of the usual situation. What had happened was that the Ground Grid in the substation and the surrounding area (including the Unit 1 Main Power Transformer) had become hot. What do you do when the ground grid becomes charged?
The Ground Grid is what is supposed to protect you when a surge happens, but what happens when the ground grid itself is the problem? In this case, when the high voltage line about 60 feet from the telephone cable surge protector, arced to ground, it fed a tremendous amount of power back through the ground grid. when equipment detected the surge in voltage, they automatically defaulted their circuits to ground. That’s why the telephone circuit died. That’s what tripped the Main Power Transformer.
When the telephone circuit detected the high voltage surge, it shorted to ground (which was the problem), causing the high voltage to feed directly into the phone line and down the line to the next Southwestern Bell relay switch, which also defaulted to ground, trying to bleed off the surge as it went from relay switch to switch until enough of the power was able to be diverted to ground.
That day sure turned out to be a learning experience. I learned that when all the lights go out in the control room, that it is almost assured that the coffee pot in the electric shop is going to stop working. I also learned that in order to coax the plant manager to the electric shop, a major electrical tragedy is one good way. I learned that when shooting rusty water into the air don’t point it at a high voltage auxiliary substation switch. — I’m sure Mickey Postman learned that lesson too. I also learned that just like in Star Trek… whenever there is a dangerous job to do, the Captain is always the one that wants to do it. Does that make sense? Send a Peon like me in there…
I also learned something else about Power Plant Men…. You see…. People like Dale Mitchell, George Alley and Mickey Postman all are examples of incredibly wonderful Power Plant Men. When they were out there doing their duty and something tragic like this, all the Power Plant Men felt their pain. They knew that they all felt guilty for tripping the unit. It didn’t matter that a million dollars every so many minutes was walking out the door in revenue. The only thing that mattered was that these three men were safe.
Since I have left the Power Plant, I have found that the idea that the employee is the greatest asset that a company can possess is not a universal idea. You see, there was never the thought that any of these people should be fired for their mistake. On the contrary. The true Power Plant Men did whatever they could to let them know that they knew exactly how they felt. It could have happened to any of them.
Besides the friendship between Power Plant Men, one of the things I miss most about working at the Power Plant is that the employees are held in high esteem as a real asset to the company. Many could learn from their example.
Comments from the Original post
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I like the mix of storytelling and information sharing you deliver here. Thanks again
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Aug 8, 2011 I lost all reserve in and lost both units in 2 separate storms and A1 would not start for a few minutes and A2 was leaking antifreeze terribly not a scratch and back online in 34 hours both units and no one ever asked me one question even with a Safety Dept not one question asked of me the SS on duty. Not many men on the planet have ever experienced an uncontrolled total plant outage- you would of thought a learning opportunity would of took place. Feb 2011 worst winter temps in years 50 Units or more tripped in Texas let alone the trusty units of Redbud and McClain were fighting Sooner rolled right along with storm warnings for two weeks ahead – the ICS still went to Detroit for just tours of other facilities once again the fall guy Tarver McArthur stood alone. I had authored a Freeze Protection Plan for the plant and that seemed to save the day and explain to the regulatory bodies how we were online and everyone else in Texas was off and enjoying rolling blackouts in a terrible winter weather situation not to mention our powers that be were all stranded in Detroit and very few people could get to the plant without getting stuck trying to get there as well – but a few health heart issues later I am still here to tell about it all you would think folks would want to take advantage of someone that had went through the fire and Ice but thats ok I want them someday distant to get all the credit they deserve when the trumpets sound as that is truly what matters most. DT
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Great story, and yes, you took exactly the proper lesson from it, and it is too bad that many of our bosses haven’t learned it.
And yup, I’ve buried a lot of electrocuted squirrels over the years.
Rivers and Rose in the Power Plant Palace
Originally posted January 25, 2013:
When is the appropriate time to call 911? Calling 911 in the Power Plant is when you call the Shift Supervisor to report something important. As Randy Dailey, our Safety Trainer extraordinaire, always taught us, first tap the person on the shoulder and say, “Are you all right?” Then you point your finger at someone and say, “Call 911!” That’s called “Activating the EMS” (Emergency Medical System). Besides medical emergencies, there are other reasons to call the Shift Supervisor.
I learned early on to ‘fess up when you have done something wrong.” People appreciate it when you tell them up front that you goofed. That way the problem can be dealt with directly. Dee Ball was that way. Any time he wrecked a truck, he didn’t hesitate to tell his boss. So, even as a summer help I had developed this philosophy. Never be afraid to expose your blunders. It works out better in the long run.
One example of someone not following this philosophy was Curtis Love. As I mentioned in the post Power Plant Spider Wars and Bugs in the Basement, Curtis didn’t want to tell anyone that he had been bitten by a brown recluse for the third time because he was afraid of losing his job.
His philosophy came back to bite him a year and a half later when he was on the labor crew when he was the designated truck driver. I had moved on to the electric shop by this time.
He was backing up the crew cab around a corner under the Fly Ash hoppers up at the coalyard when the side of the crew cab came into contact with one of those yellow poles designed to protect the structure from rogue vehicles. Unfortunately. This created a dent in the side of the truck.
Curtis, already on probation. worried that he would be fired if he told anyone about this mishap, failed to tell Larry Riley about this incident. Larry, on the other hand, was standing in front of the Coalyard Maintenance shop (the labor crew home), and saw the entire incident. At that moment, he turned to one of the labor crew hands and said, “I hope Curtis comes over here and tells me about that.” Unfortunately, Curtis decided to act as if nothing had happened. This resulted in his termination. As much as I cared about Curtis, I must admit that the Power Plant scene was probably not the best location for his vocation.
I had seen Dee Ball do the same thing over and over again, and he always reported his accidents immediately. He was never punished for an accident, though, for a number of years, he was banned from driving a truck. You can read more about this in the post: Experiencing Maggots, Mud and Motor Vehicles with Dee Ball.
One day during the summer of 1984 just after lunch, 1A PA fan tripped (PA stands for Primary Air). When this happened, number one unit had to lower it’s output from over 500 Megawatts down to around 200. The trip indicator on the 6900 volt breaker said that it had been grounded. Being grounded means that one of the three phases of the motor or cable had made a circuit with the ground (or something that was grounded). The trip circuits shut the fan down so fast that it prevents an explosion and saves the fan from being destroyed.
Diana Lucas (later Diana Brien), Andy Tubbs and I were given the task of finding the ground and seeing what we could do to fix it. We unwired the motor, which was no easy task, because the motor is about the size of a large van, and about 10 times heavier.
So, we spent the rest of the day unwiring the motor (in the rain), and unwiring the cable to the motor from the breaker in the main switchgear and testing both the motor and the cable with various instruments looking for the grounded wire or coil that caused the motor to trip. We used a large “Megger” on the motor. It’s called a Megger because it measures Mega-Ohms. So, it’s technically called a Mega-Ohm meter. Ohms is a measurement of resistance in an electrical circuit. We usually use a small hand cranked megger, that is similar to an old hand crank telephone that generates a high voltage (good for shocking fish in a lake to make them rise to the surface). In the case of the hand cranked Megger, it would generate 1,000 volts.
The Megger this size would have been useless with this large motor. Instead we used one that was electric, and you ran the voltage up over 10,000 volts and watched the mega-ohms over a period of 1/2 hour or so.
For the cables, we hooked up a Hypot (or Hipot). This stands for High Potential. Potential in this case is another word for “Voltage”. It would charge up and then you pressed a button and it would send a high voltage pulse down the cable, and if there is a weak spot in the insulation,The Hypot will find it. So, we hooked a Hypot up to the cable and tried to find the grounded wire. No luck.
After spending 4 hours looking for the grounded cable or motor, we found nothing. We spent another hour and a half putting the motor and the breaker back in service. The Fan was put back into operation and we went home. As I was walking out to the car with Bill Rivers, he told me, “I knew they weren’t going to find anything wrong with that fan.” He had a big grin on his face.
At first I thought he was just making an educated guess as Rivers was apt to do on many occasions (daily). It was raining and I could see where water may have been sucked into the motor or something and had momentarily grounded the motor. Just because we didn’t find anything didn’t mean that the breaker didn’t trip for no reason.
When we were in the car and on our way to Stillwater, Oklahoma with Yvonne Taylor and Rich Litzer, Bill explained that he knew why the motor tripped. He had been walking through the main switchgear with Mike Rose, and Mike, for no apparent reason other than curiosity, had opened up the bottom door to the breaker for 1A PA fan. He looked at it for a moment and then slammed the door shut. When he did this, the breaker tripped.
So, the ground relay happened to be the one that tripped. It might as well been an over-current or a low voltage trip. It just happened to trip the ground trip. Bill said that he told Mike that he should call the Shift Supervisor and let him know so they could restart the motor. Mike on the other hand told Bill that he was already on probation and was afraid of losing his job if he reported that he had slammed the door on the breaker and tripped the fan.
If there was ever a reason to call 911, it was then. All he had to do was tell them, “I accidentally tripped the PA fan when I bumped the breaker cabinet.” They would have told him to reset the flag, and they would have started the fan right back up. No questions asked… I’m sure of it. And they wouldn’t have lost their generating capacity for the remainder of the afternoon and we wouldn’t have spent 4 hours unwiring, testing and rewiring the motor in the rain with a plastic umbrella over our head.
Bill wasn’t about to tell on Mike. If Mike didn’t want to report it, Bill wasn’t going to say anything, and I understand that. I probably would have kept it to myself at the time if I was in Bill’s shoes (I’m just glad I wasn’t because I probably wouldn’t have been able to sleep soundly for the next year). But 30 years later, I might write about it in a Blog. Even though I wouldn’t have looked to Mike to teach me much about being an electrician (he was more of an Air Condition man anyway), I still loved the guy.
Mike died almost two years ago on May 29, 2011. He was from England and had lived in Canada for a time. He used to work on trains. Trains, even though they are diesel, are really electric. The Diesel engine really runs a generator that generates electricity that runs the train. I know that Mike was a good man at heart. He loved his family with all his heart. Here is a picture of the Limey:
Ok. So I know what you are thinking…. There must be a story about myself in here somewhere. Well, you would be right. First of all. I always ‘fessed up to my mistakes, as my current manager at Dell knows well (yes. I still mess up after all these years). I told my current manager the other day that CLM was my middle name. (CLM means “Career Limiting Move”). So here is my power plant “mess up” story (well one of them):
In January 1986, I returned from my Honeymoon with my new wife Kelly when I found that we had hired a new electrician. Gary Wehunt was replacing Jim Stephenson who had left the plant on February 15, 1985, which is a story all it’s own. We had just started an overhaul on Unit 1.
I remember the first Monday I spent with Gary. It was January 6, 1986 and we were working on cleaning out the exciter house on the end of the main power generator with Diana Brien (formerly Diana Lucas). We were discussing salaries and Gary was surprised to find out that I was making more than he was. Well… I had been an electrician for over 2 years and had been promoted regularly…. so I didn’t think there was anything strange about it, except that I still looked like I was only about 18 years old (even though I was 25) and Gary was about 34. I had already been promoted 4 times and my salary had gone from $7.15 to over $12 an hour.
Anyway, when that first Wednesday rolled around, Since Gary and I were assigned to Substation Inspection that week, (Some later time I may go into the details of what “Substation Inspection” entails), but for now, let’s just stick with my “911 call.” It is enough to say that we were in the main plant substation relay house on Wdnesday January 8, 1986 at 9:00 am. One of our jobs was to call other substations and perform a test called a “Transfer Trip and Carrier Test”. We had called Woodring Substation (Woodring is a town in Oklahoma and we had a 345 KV line going there), and I was talking to the man in the substation on the other end of the phone line.
At the same time I was showing Gary just how experienced I was at being an electrician. People had told me that you had to be a plant electrician for 5 years before you really became a “first class” electrician. Well. Here I was at 2 years, and I thought I was so good that I could do anything by now…. — Yeah… right. I told the guy on the other end of the line as I turned a switch…. Amber light… Back to Blue…. and I wrote down the value on the meter (paperwork… oh yes…. it’s that important. Like A-1 sauce).
Then I reached for the second switch. I said, “Carrier test”, then turned the switch. The lights in the relay house went out and we were in the dark. I told the guy on the other end of the line….. “Well. That’s not supposed to happen.” Then as I let go of the switch and it returned to it’s normal position, the lights turned back on. Okay……
I wrote the numbers down from the meter and said goodbye to the other faceless substation man on the other end of the line that I talked to over 100 times, but never met in person. He sounded like a nice guy. Then I headed for the gray phone. I heard the Shift Supervisor paging Leroy Godfrey (The Electrical Supervisor) on line 2 (we had 5 Gray phone lines. The Gray Phone was our PA system).
When I picked up the line I heard Leroy pick up the phone and the Shift Supervisor tell Leroy that we just lost station power in the main substation and it had switched over to Auxiliary power. I immediately jumped in and said, “Jim (for Jim Padgett, the Shift Supervisor), I did that. I was performing a Carrier test with Woodring and the moment I performed the carrier test the lights went out.” Leroy chimed in by saying, “That wouldn’t cause you to lose station power.”
Well, in my ‘inexperienced’ plant electrician way, I responded, “Well. All I know is that when I turned the switch to perform the carrier test, the lights went out, and when I let go of the switch, the lights came back on.” Leroy reiterated, “That wouldn’t cause you to lose station power.” I replied with, “I’m just saying….” and left it at that. I had done my job. They knew I was out here. They knew I had called 911 right away. I explained what I was doing…. they could take it from there.
I had hoped that I had showed Gary upfront that it doesn’t hurt to report your mistakes (even though I hadn’t made one as far as I could tell), but I was 100% sure I had done something to cause the relay house to lose power. Though, I couldn’t figure out why.
After lunch, Bill Bennett, our A foreman came down to the shop to tell me that they figured out how the substation lost station power. He said that a road grader had been grating the road down by the Otoe-Missouri reservation (which is actually called “Windmill road” I guess because there is a windmill down that road somewhere), and had hit an electric pole and knocked it over and had killed the power to the substation.
It turned out that the substation relay house was fed by a substation down that road where we have a radio tower. So, think about this. The exact time that I turned that switch in the substation, a road grater 2 1/2 miles away hits a telephone pole accidentally and knocks it to the ground and kills the power to the substation at the exact same time that I am performing a transfer-trip and Carrier test with Woodring Substation, and the time it takes to switch to auxiliary power is the exact time it took me to let go of the switch.
Don’t tell me that was by accident. I will never believe it. I think it was for the soul purpose of teaching me a useful lesson or two. First….. don’t be afraid to tell someone when you do something wrong. Second…. If you think you have control over the things that happen to you in your life… well, think again…… Third….. God watches you every moment, and if you let him, he will guide you to do the right thing when the time comes. Oh, and Fourth: “Doesn’t God have a great sense of humor?”
God bless you all.
COMMENTS FROM THE ORIGINAL POST:
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Monty Hansen January 26, 2013
I had a similar thing happen to me, I was upgrading to shift foreman & system called to remove a tag in the switchyard & put the switch back to auto. The tag on the pistol grip was attached with a plastic zip tie & the previous operator had put it on real tight, as I was wrestling it off with my leatherman, the pliers slipped & I banged my elbow into the control panel, at that very instant there was a loud BANG as several 345 KV breakers opened simultaneously in the switchyard, I had the phone pinched between my shoulder & ear as I was wrestling with this switch & talking to the system control operator, he said a few bad words – gotta go – & hung up. The power plant lost all power & went in the black, I, of course was just sick in the pit of my stomach, after we got power restored, the plant back on etc. I called system back to see if they found the cause & fess up to causing the trip (I figured I must have caused a trip relay to close when I hit the panel) – anyway a crane at a plant down the road had got it’s boom tangled in the power line & went to ground – AT PRECISELY THE INSTANT MY ELBOW SLIPPED & HIT THE PANEL!!
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Ron Kilman January 26, 2013
Some great illustrations of the truth in Proverbs 28:13 “He who conceals his transgressions will not prosper, But he who confesses and forsakes them will find compassion”.
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justturnright January 28, 2013
CLM: I can relate.
My first boss 30 years ago once told me he was going to officially nickname me “I’m sorry” (and make me wear it for a name badge) if I said it one more time.
Hey, there’s worse things.
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Roomy January 29, 2013
I had not thought about Mike Rose in years. He was a good guy to work with, now Rivers was a different story!!!
Sub checks, I used to love to do sub checks. I performed pilot wire & transfer trip checks for years. I hated it when they went to being done by automation.
Thanks for bringing back old memories.
Petty Power Plant Jokes Played on Prominent Power Plant Men
Originally posted September 13, 2013:
Of the 1,500 jokes played on Power Plant Men while I was working at the Coal-fired Power Plant in North Central Oklahoma, I can only remember a handful of the smaller ones. There are some I’m saving for later topics. Sometimes it was the smallest jokes that spoke the loudest. Especially when great care was taken to play the joke just right.
I think it was the idea that someone thought enough of you to spend a great deal of time setting up a joke just for the one little moment that the person finally realizes that they have been played. It’s when that smile comes across their face that all that work pays off. The realization that someone else would spend so much time just to make you smile was a good indication that they really did care about you.
In the post called, “Why Stanley Elmore and Other Power Plant Questions” I told a story about when I was a janitor in the electric shop and one of the electricians Andy Tubbs had been playing jokes on me while I was cleaning the bathroom. The funniest one was when I had turned around for a moment and when I went to go grab the dust mop, the handle to the mop was missing, while the dust mop was just sitting there on the floor. The handle was propped against the wall across the shop while Andy was innocently looking at a blueprint. It was so funny I had to go in the bathroom where I literally laughed out loud.
Charles Foster, my electric foremen had told me of a time when he played a joke on a welder in the welding shop that was welding away on something. The power to the welding machine was around the corner. Charles picked up the cord for the welder and kinked it like you would kink a water hose to stop the water from flowing. When he kinked it, the welding machine stopped working.
The welder looked at the machine to find that the power was off. Then he looked over and saw that Charles was standing about 40 feet away grinning at him holding the kinked cable. About that time, Charles straightened out the cable and the welding machine turned back on. The welder spun around to find the welding machine humming away. He looked back at Charles who kinked the cable again and the welding machine again shut off.
Amazed, the welder said something like, “I didn’t know you could do that!” Charles shrugged, dropped the cable and walked off. Unbeknownst to the welder, as Charles left, he met up with the other electrician that had been opening an closing the electric disconnect where the welding machine received its power. Leaving the welder unaware.
In the electric shop there is one bathroom. It is shared by all electricians, and therefore it has a lock on the door because Diana Lucas (Brien) had to use it. But sometimes someone might not realize that it was used jointly by both male and female members of the Power Plant family, and they might not lock the door. So, on occasion, Dee would go into the bathroom only to find that it was already occupied.
Once she entered the bathroom and found that someone was in the stall. She waited around for a while and asked me to go check it out because the guy was taking quite a long time and what at first was only a minor inconvenience was becoming higher priority. So, I entered there bathroom and sure enough. The stall was closed and there was a pair of boots easily visible under the stall where someone sat taking their own sweet time.
Dee finally figured that it wasn’t worth the wait and walked across the T-G floor to the maintenance shop to the nearest women’s restroom. After a while someone else remarked that someone was in the bathroom and had been in there a long time. At that point, it became obvious that either someone had died while sitting on his thinkin’ chair, or something else was definitely amiss.
So, one of the electricians decided to see if everything was all right. That was when they peered into the stall to find that there was only a pair of boots sitting all by themselves in the stall. It turned out that O D McGaha had put them there. He locked the stall, then climbed out under the stall and left them there. — It was a pretty good joke. It had half the shop concerned about the mysterious stranger in the stall.
Soon after this episode, a new sign was placed on the bathroom door:
Other little jokes like that were played on individuals throughout the 20 years that I worked at the plant. One small one that is a typical example of many was when Mickey Postman drove to work one morning with a brand new motorcycle. He was really proud of the new machine. Well. Mickey’s nickname at the time was “Pup”.
Mickey had two main reasons why he was a prime target for having jokes played on him. First, he took the jokes pretty well, because he would have a definite reaction. Sometimes good. Sometimes not so. The second reason was that he was red-headed. That meant that when he realized that a joke was being played on him, his face would turn as red as his hair. Everyone witnessing this couldn’t help but smile.
Mickey had worked his way into the maintenance shop from a janitor as I had, though he missed the labor crew (I believe) because it hadn’t been dreamed up by Ray Butler yet. He and I were practically the same age. He is 7 months older than I am. So, I always felt like, “but for the grace of God go I”. No. I don’t really mean it. I care a lot for Mickey and I never personally considered him as a candidate for jokes. I guess it was because he already had a cohort of Power Plant Men willing to play that part.
So, anyway. Mickey had this shiny new motorcycle parked out in the parking lot all day, so it was inevitable that at least one of the many Power Plant Men that had been assigned to the “Play a Joke on Mickey” detail, would happen to pass by the motorcycle in the parking lot. One of them would have felt obligated to reach down and turn the gas valve off.
The word had gone out throughout the plant that the valve had been closed on Mickey’s motorcycle so that we were all to expect that about the time that Mickey hit the bridge over the discharge on the way out the gate, his motorcycle would run out of fuel and die. It’s times like this that you never forget. A simple joke. A couple hundred Power Plant men all chuckling as they drove across the discharge bridge grinning at Mickey trying to restart his brand new motorcycle that had died perfectly positioned midway across the bridge. His face beaming as red as his hair!
I won’t go into the Wedding present that was given to Mickey Postman the day before his wedding. I intended this post to be only about petty or “minor” jokes. That one was a doozy. Actually. I will never post anything about it, other than to say that I wouldn’t ever say anything about how the machinist’s blue dye was applied.
Machinist’s Blue Dye, or Layout fluid is used when honing down a surface to make sure it is flat. There are other uses for it, but that is the one I am most familiar with. I wonder how that blue color looked along with Mickey’s red face…
Here are examples of two small jokes that took a lot of preparation.
The first one involved Howard Chumbley’s chair. Howard was a foreman in the electric shop. One of the nicest Power Plant Men in all of God’s creation. He was shorter than most taller people. And he was particular about how high his chair was adjusted. Being particular about anything automatically meant that you were a prime target for a joke dealing with whatever you were particular about.
Back then (1984), the height of an office chair was adjusted by turning it upside down and spinning the wheel bracket around to screw in or out the shaft.
So, Charles and I would rotate the bottom of the wheels around 1/4 turn each day. That meant just moving the wheels around to one set of wheels. Not very much. Every week the bracket would only be turned about 1 time, especially given that we wouldn’t remember to do it every day.
Eventually, after 5 or 6 weeks, Howard would go to sit down in his chair and realize that it was lower than he would like it to be. So, he would turn it over and lay the seat on his desk and spin the wheel bracket around a few times. Then test it and do it again until it was just the right height. Howard probably never thought about why every month and a half or so, his chair would be too short and he would end up turning it over and adjusting it back up.
This was a joke that Howard never knew was being played, but every time that chair went upside down, you can bet that Charles and I were grinning from ear-to-ear to have been there to watch it.
Ok. the last story has to be about Gene Day. After all. There was no one that I loved playing jokes on more than Gene Day. Actually, half of them, Gene probably never knew had been jokes. I have written two posts about playing jokes on Gene Day. One of them was just about one joke. See “Psychological Profile of a Control Room Operator” and “Power Plant Humor and Joking with Gene Day“.
So, this particular week, I noticed that Gene Day was the auxiliary operator for Unit 1 Boiler. That meant that at least once each shift he was going to walk through the Unit 1 Precipitator Control Room that housed the controls for the 84 transformers on the precipitator roof.
So, I decided, this was a perfect opportunity to play a petty joke on Gene Day. I took an Eeprom chip that was used to hold the control program for a Precipitator control cabinet, and proceeded to rewrite the program.
I found the code in the assembly language code that sent the message to the display when there was an overcurrent trip. That is, when the cabinet trips, the little LCD display would say: “Overcurrent Trip”. I rewrote the code to say: “Gene Day Trip”. This meant finding the code string: 4F:76:65:72:63:75:72:72:65:6E:74:20:54:72:69:70 and replacing it with: 47:65:6E:65:20:44:61:79:20:54:72:69:70:20:20:20. I wrote the program for a specific cabinet in the middle of the precipitator that I could trip without causing an issue in the general operation of the precipitator.
Then I took the chip to the Precipitator Control room and replaced the control chip for that cabinet and left it running. I had seen Gene Day on his way to the Precipitator Control room the day before, so I had a pretty good idea what time he would be passing through. Because no matter how lazy Gene Day was, he was always consistent. (Gene you know I’m kidding…. right?)
Anyway. I spied Gene leaving the control room around the time I expected, so I made haste to the Precip. Control Room and with my screwdriver, after opening the cabinet, I reached down to the tripping mechanism for an overcurrent trip and I tripped the cabinet. Then leaving from the opposite direction that Gene would be arriving, I slipped out of the Precip Control Room and headed for the plant control room to see Gene’s reaction when he arrived.
About the time I was going around the corner in the breezeway toward the Unit 1 elevator, I saw that Gene had already exited the precip. area, so when I entered the T-G basement I quickly called Gene on the gray phone. Gene turned around and went back in the Precip switchgear (which was just below the control cabinets).
When Gene answered the phone I told him that I was looking at the Precipitator controls in the control room and I saw that one of the cabinets had tripped and I was wondering if he had just been out there because the error indicated something very strange. He said he had just been in there and hadn’t noticed that a cabinet had tripped.
So, I asked him if he could look again, it was 1D8. I needed to know what the cabinet display said had happened because it looked like Gene had done something to it. He told me he hadn’t touched anything, but he would go look. — of course, when he went to look at it, the display showed: “Gene Day Trip”.
So, I was sitting at the precipitator computer for Unit 1 when Gene Day arrived in the Control room. As was typical with Gene Day, my head began to waiver and my eyes began to blur as Gene had grabbed me by the throat and was shaking me back and forth. My eyes may have been blurry, and I know that I was acting totally surprised as if I didn’t know what had happened, but you can believe that inside I was grinning ear-to-ear!
Comment from original post:
September 21, 2013:
Folks will go to elaborate lengths and great effort to perform jokes like these on fellow workers while feeling put-upon and resentful at something half the trouble requested done by the boss… We are a funny species!
More comments from the last repost:
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“Folks will go to elaborate lengths and great effort to perform jokes like these on fellow workers while feeling put-upon and resentful at something half the trouble requested done by the boss… We are a funny species!” Keeps it entertaining, right? 🙂
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I’ve been following your blog, and in the early a.m. after I’ve gotten the coffee started and my husbands lunch prepared and breakfast fixed, then I sit down to relax and I read your stories, I start laughing, sometimes really hard, and my husband looks at me like I’ve fallen off my rocker!!! What a good way to wake up in the mornings. Thank you for sharing. May God bless you today!
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Cool stories. Workplaces should be like this. I think this is something that is lost on people these days, that you need to laugh.
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I love these stories!
OK Kevin – how could you remember those lines of Eeprom code from 30 years ago?
Also, I know somebody is playing a joke on me (like what you did to Howard Chumbley). My bathroom scales are going up about 1 pound every week. Can’t figure out who’s responsible yet 😦-
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The code is easy to remember: “Overcurrent trip” is translated into ASCII numbers. Where a capital A is 65 and a small A is 97 and then just count up from there. So, the capital O is the ASCII number 79 which when converted to a Hexidecimal number is 4F (16 goes into 79 4 times, with 15 left over. An F represents the number 15). So, “Overcurrenct trip” becomes: 4F:76:65:72:63:75:72:72:65:6E:74:20:54:72:69:70. “Gene Day Trip” is three characters shorter than Overcurrent trip, so, I had to add extra spaces at the end, which are the three “20”s (an ASCII number of 32) on the end of 47:65:6E:65:20:44:61:79:20:54:72:69:70:20:20:20. in order to keep the addresses on the chip consistent.
Another note is that each two digit Hexidecimal code is equal to 8 bits which is a byte. You can determine what each byte is by taking each digit of the Hex number and translating it into 4 binary digits. So… 1 is 0001, 2 is 0010, 3 is 0011, 4 is 0100, 5 is 0101, 6 is 0110, 7 is 0111, 8 is 1000, 9 is 1001, A is 1010, B is 1011, C is 1100, D is 1101, E is 1110, F is 1111
So, the Hex number for a Capital O is 4F, and that indicates an 8 bit byte of: 01001111
And that’s how computers interpret the world. Zeroes and One’s. Or On and Off. So, if there is voltage on the first bit it is a 1 if the voltage is missing, it is a 0.
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So funny! We used to have fun like this on the volunteer fire department. Always makes the tough stuff better when you can laugh together.
Runaway Fire Hydrant Leaves Power Plant in the Dark
Originally posted May 17, 2014:
Don’t believe it when the Electric Company tells you that the reason your town lost electricity for an hour was because a squirrel climbed onto a transformer and shorted it out. The real reason just may be more bizarre than that and the company doesn’t want you to know all the different creative ways that power can be shut off. This is a tale of just one of those ways. So, get out your pencil and paper and take notes.
One spring day in 1993 while sitting at the Precipitator computer for Unit one at the Coal-fired Power Plant in North Central Oklahoma, while I was checking the controls to make sure all the cabinets were operating correctly, suddenly there was a distant boom, and the lights in the control room went out. The computer stayed on because it was connected to an electric panel called the VSP or Vital Services Panel, which in turn was supplied by the UPS system (Uninterruptible Power Supply). That was one of those moments where you may pause for a moment to make sure you aren’t still at home dreaming before you fly into a panic.
The Precipitator cabinets all indicated on the computer that they had just shutdown. I rose from the chair and walked around to the front of the Alarm Panel for Unit one, and found that the fluorescent lights were only out on Unit 1. The lights were still on for Unit 2. The Control Panel was lit up like a Christmas Tree with Green, Red, Blue and Yellow Lights. The Alarm Printer was spewing out paper at high speed. As the large sheets of paper were pouring out onto the floor, I watched as Pat Quiring and other brave Power Plant Control Room operators were scurrying back and forth turning switch handles, pushing buttons, and checking pressure gauges.
Just this site alone gave me confidence that everything was going to be all right. These Control Room operators were all well trained for emergencies just like this, and each person knew what their job was. No one was panicking. Everyone was concentrating on the task at hand.
Someone told me that we lost Unit 1, and the Auxiliary Power to Unit 1 at the same time. So, Unit 1 was dead in the water. This meant, no fans, no pumps, no lights, no vending machines, no cold water at the water fountain and most importantly, no hot coffee!!! I could hear steam valves on the T-G floor banging open and the loud sound of steam escaping.
I turned quickly to go to the electric shop to see what I could do there in case I was needed. I bolted out the door and down the six flights of stairs to the Turbine-Generator (T-G) basement. Exiting the stairway, and entering the T-G basement the sound was deafening. I grabbed the earplugs that were dangling around my neck and crammed them into my ears. Steam was pouring out of various pop-off valves. I ducked into the electric shop where across the room Andy Tubbs, one of the electric foreman was pulling large sheets of electric blueprints from the print cabinet and laying them across the work table that doubled as the lunch table.
When I asked Andy what happened, I learned that somehow when a crew was flushing out a fire hydrant the water somehow shot up and into the bus work in the Auxiliary Substation (that supplies backup power to the Power Plant) and it shorted out the 189,000 volt substation directly to ground. When that happened it tripped unit 1 and the auxiliary substation at the same time leaving it without power.
I will explain how a fire hydrant could possibly spray the bus work in a substation in a little while, but first let me tell you what this meant at the moment to not have any power for a Power Plant Boiler and Turbine Generator that has just tripped when it was at full load which was around 515 Megawatts of power at the time.
Normally when a unit trips, the boiler cools down as the large Force Draft (FD) Fans blow air through the boiler while the even larger Induced Draft (ID) fans suck the air from the boiler on the other end and blow the hot air up the smoke stack. This causes the steam in the boiler tubes to condense back into water. Steam valves open on the boiler that allow excessive steam to escape.
When the boiler is running there is a large orange fireball hovering in space in the middle of the boiler. The boiler water is being circulated through the boiler and the Boiler Feed Pump Turbines are pumping steam back and forth between the turbine generator and the boiler reheating the steam until every bit of heat from the boiler that can be safely harnessed is used.
When all this stop suddenly, then it is important that the large fans keep running to cool down the steam, since it is no longer losing energy in the generator as it was when it was busy supplying electricity to 1/2 million people in Oklahoma City. The power is fed to the fans from the Auxiliary substation located right outside the Main Switchgear where all the breakers reside that supply the power to the fans. Unfortunately, in this case, the Auxiliary substation was shutdown as well, leaving the boiler without any fans.
Without fans for cooling, and pumps to circulate the water, the walls of the boiler began heating up to dangerous temperatures. Steam was whistling out of pop off valves, but if the steam drum on the top of the boiler were to run dry, then the entire boiler structure could be compromised and begin melting down. — So, this was serious. Something had to be done right away. It wouldn’t be as bad as the China Syndrome since we were burning coal instead of nuclear power, but it would have caused a lot of damage nonetheless.

From the movie “The China Syndrome” where a similar emergency existed only in the movie, it was a Nuclear Plant
I have a side story about this picture, but I think I’ll save it for another post because I don’t want to digress from the main story at this point (Ok. Let me just say “Jack Maloy and Merl Wright” for those who can’t wait) See the post: “Power Plant Conspiracy Theory“.
With the prospect that the boiler might melt to the ground in a pile of rubble, it would seem that the main priority was to turn the Auxiliary Substation back on so the fans could be turned back on and prevent the boiler from collapsing. So, we walked out to the substation and looked at the switches that would have to be operated in order to first power up the main bus and then to close to supply power to the two big transformers and the six smaller transformers that supplied the Unit 1 Main Switchgear.
While inspecting the switches where the electricity had gone to ground we found that one of the main insulators was cracked.
Since this insulator was cracked, we didn’t really want to operate the switch to test if another 189,000 volts would go straight to ground again, especially since one of us would be standing right underneath it cranking the switch. So, we went back to the shop to find an alternative.
By this time the Plant Manager, Ron Kilman arrived in the shop, and understanding the urgency to find a solution asked us what were the alternatives. He was relying on our expertise to make the decision.
The other solution would be to cut the power over from Unit 2 which was still humming away pushing electricity to Oklahoma City out of the 345,000 volt substation. The cut over would be very simple because the switchgear was designed with this in mind. We analyzed the power rating on the auxiliary transformers on Unit 2 and thought that we might be cutting it close to have them running both sets of fans at the same time, especially since the full load amps of a huge fan starting up was about 10 times the normal rate.
The transformer was rated to handle the load, but consider this. What if this caused Unit 2 to trip as well. With the Auxiliary substation offline, if Unit 2 tripped, we would be in twice the amount of trouble we were currently in. What a day it would have been if that had happened and two 250 foot boilers had come crashing to the ground in a pile of rubble. After reading the power ratings on the auxiliary transformers I was thinking, “Yeah, let’s do it! These transformers can handle it.” Andy was not so eager.
So, we were left with one alternative. That was to shut the switch in the Auxiliary substation that had the cracked insulator and take our chances that it wasn’t going to short to ground and blow up over our heads. I think I was eager to close the switch for Andy, but if I remember correctly, he didn’t want me to be the one to suffer the consequences and decided to close the switch himself. Needless to say. Andy closed the switch, and nothing blew up.
As soon as the power was restored to the switchgear, the fans were powered up and the temperature in the boiler was quickly reduced. The coffee pot in the Electric Shop began heating the coffee again. The power plant was saved from a major catastrophe. That was delayed for another day… of which I will talk about later (see the post “Destruction of a Power Plant God).”
So, how exactly does a fire hydrant shoot water up into the bus work of a substation like the picture of the switch directly above? The culprit fire hydrant wasn’t in the substation, it sat alongside it outside the fence a good 50 feet from the high voltage switch. No hose was attached to the fire hydrant. It was only being flushed out as part of a yearly activity to go around and make sure the fire hydrants are all operating correctly.
Here is the story about how the squirrel climbed into the transformer this time….
George Alley, Dale Mitchell and Mickey Postman were going around to the 30,000 fire hydrants on the plant ground (ok. maybe not that many, but we did have a lot of them), and they were opening up the valves and flushing them out. That means, they were letting them run for a while to clear them out from any contaminates that may have built up over the year of not being used.
Throughout their adventure they had opened a multitude of Hydrants situated out in the fields along the long belt conveyor from the coalyard and around the two one-million gallon #2 Diesel tanks.
The brave Power Plant Men, learned that when opening a fire hydrant wide open in the middle of field had unintended consequences. It tended to wash out the ground in front of the flow of the water shooting out of the hydrant. So the team of experts devised a plan to place a board in front of the hydrant when it would be in danger of tearing a hole in the terrain. The board would divert the water into the air where it would fan out and not cause damage to the surrounding area.
This was working fine, and when they arrived at the fire hydrant next to the substation, since the stream from the hydrant was pointing directly into the substation (hmm. a design flaw, I think), they decided to prop the board up against the fence to keep from washing away the gravel in the substation. Well. When a fire hydrant is opened that hasn’t been used for a year, the first flow of water to shoot out is dark brown.
You may think that this is because the water has somehow become dirty over the past year, but that isn’t quite the case. What has happened is that the pipe has been rusting little by little and the water has become saturated with the rust. So, the water shooting out of the hydrant was full of rust (hence the need to flush them out).
Well. Rust is made of metal. Metal is conductive, especially when it is mixed with water. When the water hit the board, it was deflected into the air and happened to direct itself directly into the high voltage switch in the substation. This caused a circuit to the ground which, once it created an arc pumped all the electricity directly into the ground.
Normally when something like this happens it doesn’t trip the Main Power Transformer to a Power Plant.
This time it did. I know there was a few heads scratching trying to figure it out. I think I figured out what happened a little while later. You see… here is the rest of the story….
Once the unit was back online and the emergency was over, someone finally noticed that the telephone system couldn’t call outside of the plant. Well. I was the main telephone person at the time, so the control room called me and asked me to look into the problem.
I checked the telephone computer and it was up and running just fine. Internal calls could be made. Only any call outside just concluded with a funny humming sound. After checking the circuit in the Logic Room next to the Rolm Telephone Computer I headed for…. guess where….. the Main Switchgear….
In the middle of the main switchgear in the back of the room right next to the Auxiliary Substation beyond the back wall, the outside telephone line came into the plant. The first thing it did was go through a special Telephone Surge Protector.
In this picture above, the silver circular buttons on the left side are really an old style surge protector. whenever there was a power surge, the carbon connection in the surge protector would quickly melt causing the circuit to go straight to ground. Thus protecting the rest of the telephone circuit. So, if some kid in their house decides to connect the 120 volts circuit to the telephone for fun to see what would happen, this circuit would protect the rest of the phone circuits. Keep in mind that this was during the early 1990 when “Surge Protection” still was basically all “mechanical”.
Anyway, when I arrived at this panel and I checked the surge protector to the main line going out of the plant, guess what I found…. Yep. Shorted to ground. Luckily there were some spares that were not wired to anything in the panel and I was able to swap them out for the ones that had been destroyed. — These were a one time use. Which meant, if they ever had to short to ground, they had to be replaced.
Ok. Fine. After a little while, we were able to call back out of the plant, though there was still some residual noise on the line. It was like this… when you called out of the plant, the person on the other end sounded like they were buried in a grave somewhere and they were trying to talk to someone living just like in an episode of the Twilight Episode where a phone line landed on a grave and the dead person tried to call his long lost love from the past.
I didn’t give it much thought other than that I figured the 189,000 volt arc to ground must have shorted out the telephone line since the phone line ran directly under the auxiliary substation ground grid.
It wasn’t until the next morning when the Southwestern Bell repairman showed up at the plant. I knew him well, since he had been working on our phone lines since before the AT&T breakup in 1984. When I met him in the front of the electric shop, he said that he needed to check our telephone circuits. I told him that I knew that we had a problem because we had a high voltage short to ground yesterday and I found our surge protectors melted away.
He explained to me that not only was our circuit affected, but that every relay house from here to Ponca City was blown out. That’s when I realized that the problem was the reverse of the usual situation. What had happened was that the Ground Grid in the substation and the surrounding area (including the Unit 1 Main Power Transformer) had become hot. What do you do when the ground grid becomes charged?
The Ground Grid is what is supposed to protect you when a surge happens, but what happens when the ground grid itself is the problem? In this case, when the high voltage line about 60 feet from the telephone cable surge protector, arced to ground, it fed a tremendous amount of power back through the ground grid. when equipment detected the surge in voltage, they automatically defaulted their circuits to ground. That’s why the telephone circuit died. That’s what tripped the Main Power Transformer.
When the telephone circuit detected the high voltage surge, it shorted to ground (which was the problem), causing the high voltage to feed directly into the phone line and down the line to the next Southwestern Bell relay switch, which also defaulted to ground, trying to bleed off the surge as it went from relay switch to switch until enough of the power was able to be diverted to ground.
That day sure turned out to be a learning experience. I learned that when all the lights go out in the control room, that it is almost assured that the coffee pot in the electric shop is going to stop working. I also learned that in order to coax the plant manager to the electric shop, a major electrical tragedy is one good way. I learned that when shooting rusty water into the air don’t point it at a high voltage auxiliary substation switch. — I’m sure Mickey Postman learned that lesson too. I also learned that just like in Star Trek… whenever there is a dangerous job to do, the Captain is always the one that wants to do it. Does that make sense? Send a Peon like me in there…
I also learned something else about Power Plant Men…. You see…. People like Dale Mitchell, George Alley and Mickey Postman all are examples of incredibly wonderful Power Plant Men. When they were out there doing their duty and something tragic like this, all the Power Plant Men felt their pain. They knew that they all felt guilty for tripping the unit. It didn’t matter that a million dollars every so many minutes was walking out the door in revenue. The only thing that mattered was that these three men were safe.
Since I have left the Power Plant, I have found that the idea that the employee is the greatest asset that a company can possess is not a universal idea. You see, there was never the thought that any of these people should be fired for their mistake. On the contrary. The true Power Plant Men did whatever they could to let them know that they knew exactly how they felt. It could have happened to any of them.
Besides the friendship between Power Plant Men, one of the things I miss most about working at the Power Plant is that the employees are held in high esteem as a real asset to the company. Many could learn from their example.
Comments from the Original post
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That was an exciting day! Another great story. Thanks for the memories.
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I like the mix of storytelling and information sharing you deliver here. Thanks again
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Aug 8, 2011 I lost all reserve in and lost both units in 2 separate storms and A1 would not start for a few minutes and A2 was leaking antifreeze terribly not a scratch and back online in 34 hours both units and no one ever asked me one question even with a Safety Dept not one question asked of me the SS on duty. Not many men on the planet have ever experienced an uncontrolled total plant outage- you would of thought a learning opportunity would of took place. Feb 2011 worst winter temps in years 50 Units or more tripped in Texas let alone the trusty units of Redbud and McClain were fighting Sooner rolled right along with storm warnings for two weeks ahead – the ICS still went to Detroit for just tours of other facilities once again the fall guy Tarver McArthur stood alone. I had authored a Freeze Protection Plan for the plant and that seemed to save the day and explain to the regulatory bodies how we were online and everyone else in Texas was off and enjoying rolling blackouts in a terrible winter weather situation not to mention our powers that be were all stranded in Detroit and very few people could get to the plant without getting stuck trying to get there as well – but a few health heart issues later I am still here to tell about it all you would think folks would want to take advantage of someone that had went through the fire and Ice but thats ok I want them someday distant to get all the credit they deserve when the trumpets sound as that is truly what matters most. DT
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Great story, and yes, you took exactly the proper lesson from it, and it is too bad that many of our bosses haven’t learned it.
And yup, I’ve buried a lot of electrocuted squirrels over the years.
Rivers and Rose in the Power Plant Palace
Originally posted January 25, 2013:
When is the appropriate time to call 911? Calling 911 in the Power Plant is when you call the Shift Supervisor to report something important. As Randy Dailey, our Safety Trainer extraordinaire, always taught us, first tap the person on the shoulder and say, “Are you all right?” Then you point your finger at someone and say, “Call 911!” That’s called “Activating the EMS” (Emergency Medical System). Besides medical emergencies, there are other reasons to call the Shift Supervisor.
I learned early on to ‘fess up when you have done something wrong.” People appreciate it when you tell them up front that you goofed. That way the problem can be dealt with directly. Dee Ball was that way. Any time he wrecked a truck, he didn’t hesitate to tell his boss. So, even as a summer help I had developed this philosophy. Never be afraid to expose your blunders. It works out better in the long run.
One example of someone not following this philosoply was Curtis Love. As I mentioned in the post Power Plant Spider Wars and Bugs in the Basement, Curtis didn’t want to tell anyone that he had been bitten by a brown recluse for the third time because he was afraid of losing his job.
His philosophy came back to bite him a year and a half later when he was on the labor crew when he was the designated truck driver. I had moved on to the electric shop by this time.
He was backing up the crew cab around a corner under the Fly Ash hoppers up at the coalyard when the side of the crew cab came into contact with one of those yellow poles designed to protect the structure from rogue vehicles. Unfortunately. This created a dent in the side of the truck.
Curtis, already on probation. worried that he would be fired if he told anyone about this mishap, failed to tell Larry Riley about this incident. Larry, on the other hand, was standing in front of the Coalyard Maintenance shop (the labor crew home), and saw the entire incident. At that moment, he turned to one of the labor crew hands and said, “I hope Curtis comes over here and tells me about that.” Unfortunately, Curtis decided to act as if nothing had happened. This resulted in his termination. As much as I cared about Curtis, I must admit that the Power Plant scene was probably not the best location for his vocation.
I had seen Dee Ball do the same thing over and over again, and he always reported his accidents immediately. He was never punished for an accident, though, for a number of years, he was banned from driving a truck. You can read more about this in the post: Experiencing Maggots, Mud and Motor Vehicles with Dee Ball.
One day during the summer of 1984 just after lunch, 1A PA fan tripped (PA stands for Primary Air). When this happened, number one unit had to lower it’s output from over 500 Megawatts down to around 200. The trip indicator on the 6900 volt breaker said that it had been grounded. Being grounded means that one of the three phases of the motor or cable had made a circuit with the ground (or something that was grounded). The trip circuits shut the fan down so fast that it prevents an explosion and saves the fan from being destroyed.
Diana Lucas (later Diana Brien), Andy Tubbs and I were given the task of finding the ground and seeing what we could do to fix it. We unwired the motor, which was no easy task, because the motor is about the size of a large van, and about 10 times heavier.
So, we spent the rest of the day unwiring the motor (in the rain), and unwiring the cable to the motor from the breaker in the main switchgear and testing both the motor and the cable with various instruments looking for the grounded wire or coil that caused the motor to trip. We used a large “Megger” on the motor. It’s called a Megger because it measures Mega-Ohms. So, it’s technically called a Mega-Ohm meter. Ohms is a measurement of resistance in an electrical circuit. We usually use a small hand cranked megger, that is similar to an old hand crank telephone that generates a high voltage (good for shocking fish in a lake to make them rise to the surface). In the case of the hand cranked Megger, it would generate 1,000 volts.
The Megger this size would have been useless with this large motor. Instead we used one that was electric, and you ran the voltage up over 10,000 volts and watched the mega-ohms over a period of 1/2 hour or so.
For the cables, we hooked up a Hypot (or Hipot). This stands for High Potential. Potential in this case is another word for “Voltage”. It would charge up and then you pressed a button and it would send a high voltage pulse down the cable, and if there is a weak spot in the insulation,The Hypot will find it. So, we hooked a Hypot up to the cable and tried to find the grounded wire. No luck.
After spending 4 hours looking for the grounded cable or motor, we found nothing. We spent another hour and a half putting the motor and the breaker back in service. The Fan was put back into operation and we went home. As I was walking out to the car with Bill Rivers, he told me, “I knew they weren’t going to find anything wrong with that fan.” He had a big grin on his face.
At first I thought he was just making an educated guess as Rivers was apt to do on many occasions (daily). It was raining and I could see where water may have been sucked into the motor or something and had momentarily grounded the motor. Just because we didn’t find anything didn’t mean that the breaker didn’t trip for no reason.
When we were in the car and on our way to Stillwater, Oklahoma with Yvonne Taylor and Rich Litzer, Bill explained that he knew why the motor tripped. He had been walking through the main switchgear with Mike Rose, and Mike, for no apparent reason other than curiosity, had opened up the bottom door to the breaker for 1A PA fan. He looked at it for a moment and then slammed the door shut. When he did this, the breaker tripped.
So, the ground relay happened to be the one that tripped. It might as well been an over-current or a low voltage trip. It just happened to trip the ground trip. Bill said that he told Mike that he should call the Shift Supervisor and let him know so they could restart the motor. Mike on the other hand told Bill that he was already on probation and was afraid of losing his job if he reported that he had slammed the door on the breaker and tripped the fan.
If there was ever a reason to call 911, it was then. All he had to do was tell them, “I accidentally tripped the PA fan when I bumped the breaker cabinet.” They would have told him to reset the flag, and they would have started the fan right back up. No questions asked… I’m sure of it. And they wouldn’t have lost their generating capacity for the remainder of the afternoon and we wouldn’t have spent 4 hours unwiring, testing and rewiring the motor in the rain with a plastic umbrella over our head.
Bill wasn’t about to tell on Mike. If Mike didn’t want to report it, Bill wasn’t going to say anything, and I understand that. I probably would have kept it to myself at the time if I was in Bill’s shoes (I’m just glad I wasn’t because I probably wouldn’t have been able to sleep soundly for the next year). But 30 years later, I might write about it in a Blog. Even though I wouldn’t have looked to Mike to teach me much about being an electrician (he was more of an Air Condition man anyway), I still loved the guy.
Mike died almost two years ago on May 29, 2011. He was from England and had lived in Canada for a time. He used to work on trains. Trains, even though they are diesel, are really electric. The Diesel engine really runs a generator that generates electricity that runs the train. I know that Mike was a good man at heart. He loved his family with all his heart. Here is a picture of the Limey:
Ok. So I know what you are thinking…. There must be a story about myself in here somewhere. Well, you would be right. First of all. I always ‘fessed up to my mistakes, as my current manager at Dell knows well (yes. I still mess up after all these years). I told my current manager the other day that CLM was my middle name. (CLM means “Career Limiting Move”). So here is my power plant “mess up” story (well one of them):
In January 1986, I returned from my Honeymoon with my new wife Kelly when I found that we had hired a new electrician. Gary Wehunt was replacing Jim Stephenson who had left the plant on February 15, 1985, which is a story all it’s own. We had just started an overhaul on Unit 1.
I remember the first Monday I spent with Gary. It was January 6, 1986 and we were working on cleaning out the exciter house on the end of the main power generator with Diana Brien (formerly Diana Lucas). We were discussing salaries and Gary was surprised to find out that I was making more than he was. Well… I had been an electrician for over 2 years and had been promoted regularly…. so I didn’t think there was anything strange about it, except that I still looked like I was only about 18 years old (even though I was 25) and Gary was about 34. I had already been promoted 4 times and my salary had gone from $7.15 to over $12 an hour.
Anyway, when that first Friday rolled around, Gary and I were assigned to Substation Inspection. Some later time I may go into the details of what “Substation Inspection” entails, but for now, let’s just stick with my “911 call.” It is enough to say that we were in the main plant substation relay house on Friday January 10, 1986 at 9:00 am. One of our jobs was to call other substations and perform a test called a “Transfer Trip and Carrier Test”. We had called Woodring Substation (Woodring is a town in Oklahoma and we had a 345 KV line going there), and I was talking to the man in the substation on the other end of the phone line.
At the same time I was showing Gary just how experienced I was at being an electrician. People had told me that you had to be a plant electrician for 5 years before you really became a “first class” electrician. Well. Here I was at 2 years, and I thought I was so good that I could do anything by now…. — Yeah… right. I told the guy on the other end of the line as I turned a switch…. Amber light… Back to Blue…. and I wrote down the value on the meter (paperwork… oh yes…. it’s that important. Like A-1 sauce).
Then I reached for the second switch. I said, “Carrier test”, then turned the switch. The lights in the relay house went out and we were in the dark. I told the guy on the other end of the line….. “Well. That’s not supposed to happen.” Then as I let go of the switch and it returned to it’s normal position, the lights turned back on. Okay……
I wrote the numbers down from the meter and said goodbye to the other faceless substation man on the other end of the line that I talked to over 100 times, but never met in person. He sounded like a nice guy. Then I headed for the gray phone. I heard the Shift Supervisor paging Leroy Godfrey (The Electrical Supervisor) on line 2 (we had 5 Gray phone lines. The Gray Phone was our PA system).
When I picked up the line I heard Leroy pick up the phone and the Shift Supervisor tell Leroy that we just lost station power in the main substation and it had switched over to Auxiliary power. I immediately jumped in and said, “Jim (for Jim Padgett, the Shift Supervisor), I did that. I was performing a Carrier test with Woodring and the moment I performed the carrier test the lights went out.” Leroy chimed in by saying, “That wouldn’t cause you to lose station power.”
Well, in my ‘inexperienced’ plant electrician way, I responded, “Well. All I know is that when I turned the switch to perform the carrier test, the lights went out, and when I let go of the switch, the lights came back on.” Leroy reiterated, “That wouldn’t cause you to lose station power.” I replied with, “I’m just saying….” and left it at that. I had done my job. They knew I was out here. They knew I had called 911 right away. I explained what I was doing…. they could take it from there.
I had hoped that I had showed Gary upfront that it doesn’t hurt to report your mistakes (even though I hadn’t made one as far as I could tell), but I was 100% sure I had done something to cause the relay house to lose power. Though, I couldn’t figure out why.
After lunch, Bill Bennett, our A foreman came down to the shop to tell me that they figured out how the substation lost station power. He said that a road grader had been grating the road down by the Otoe-Missouri reservation (which is actually called “Windmill road” I guess because there is a windmill down that road somewhere), and had hit an electric pole and knocked it over and had killed the power to the substation.
It turned out that the substation relay house was fed by a substation down that road where we have a radio tower. So, think about this. The exact time that I turned that switch in the substation, a road grater 2 1/2 miles away hits a telephone pole accidentally and knocks it to the ground and kills the power to the substation at the exact same time that I am performing a transfer-trip and Carrier test with Woodring Substation, and the time it takes to switch to auxiliary power is the exact time it took me to let go of the switch.
Don’t tell me that was by accident. I will never believe it. I think it was for the soul purpose of teaching me a useful lesson or two. First….. don’t be afraid to tell someone when you do something wrong. Second…. If you think you have control over the things that happen to you in your life… well, think again…… Third….. God watches you every moment, and if you let him, he will guide you to do the right thing when the time comes.
God bless you all.
COMMENTS FROM THE ORIGINAL POST:
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Monty Hansen January 26, 2013
I had a similar thing happen to me, I was upgrading to shift foreman & system called to remove a tag in the switchyard & put the switch back to auto. The tag on the pistol grip was attached with a plastic zip tie & the previous operator had put it on real tight, as I was wrestling it off with my leatherman, the pliers slipped & I banged my elbow into the control panel, at that very instant there was a loud BANG as several 345 KV breakers opened simultaniously in the swithyard, I had the phone pinched between my shoulder & ear as I was wrestling with this switch & talking to the system control operator, he said a few bad words – gotta go – & hung up. The power plant lost all power & went in the black, I, of course was just sick in the pit of my stomach, after we got power restored, the plant back on etc. I called system back to see if they found the cause & fess up to causing the trip (I figured I must have caused a trip relay to close when I hit the panel) – anyway a crane at a plant down the road had got it’s boom tangled in the power line & went to ground – AT PRECISELY THE INSTANT MY ELBOW SLIPPED & HIT THE PANEL!!
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Ron Kilman January 26, 2013
Some great illustrations of the truth in Proverbs 28:13 “He who conceals his transgressions will not prosper, But he who confesses and forsakes them will find compassion”.
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justturnright January 28, 2013
CLM: I can relate.
My first boss 30 years ago once told me he was going to officially nickname me “I’m sorry” (and make me wear it for a name badge) if I said it one more time.
Hey, there’s worse things.
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Roomy January 29, 2013
I had not thought about Mike Rose in years. He was a good guy to work with, now Rivers was a different story!!!
Sub checks, I used to love to do sub checks. I performed pilot wire & transfer trip checks for years. I hated it when they went to being done by automation.
Thanks for bringing back old memories.
Petty Power Plant Jokes Played on Prominent Power Plant Men
Originally posted September 13, 2013:
Of the 1,500 jokes played on Power Plant Men while I was working at the Coal-fired Power Plant in North Central Oklahoma, I can only remember a handful of the smaller ones. There are some I’m saving for later topics. Sometimes it was the smallest jokes that spoke the loudest. Especially when great care was taken to play the joke just right.
I think it was the idea that someone thought enough of you to spend a great deal of time setting up a joke just for the one little moment that the person finally realizes that they have been played. It’s when that smile comes across their face that all that work pays off. The realization that someone else would spend so much time just to make you smile was a good indication that they really did care about you.
In the post called, “Why Stanley Elmore and Other Power Plant Questions” I told a story about when I was a janitor in the electric shop and one of the electricians Andy Tubbs had been playing jokes on me while I was cleaning the bathroom. The funniest one was when I had turned around for a moment and when I went to go grab the dust mop, the handle to the mop was missing, while the dust mop was just sitting there on the floor. The handle was propped against the wall across the shop while Andy was innocently looking at a blueprint.
Charles Foster, my electric foremen had told me of a time when he played a joke on a welder in the welding shop that was welding away on something. The power to the welding machine was around the corner. Charles picked up the cord for the welder and kinked it like you would kink a water hose to stop the water from flowing. When he kinked it, the welding machine stopped working.
The welder looked at the machine to find that the power was off. Then he looked over and saw that Charles was standing about 40 feet away grinning at him holding the kinked cable. About that time, Charles straightened out the cable and the welding machine turned back on. The welder spun around to find the welding machine humming away. He looked back at Charles who kinked the cable again and the welding machine again shut off.
Amazed, the welder said something like, “I didn’t know you could do that!” Charles shrugged, dropped the cable and walked off. Unbeknownst to the welder, as Charles left, he met up with the other electrician that had been opening an closing the electric disconnect where the welding machine received its power. Leaving the welder unaware.
In the electric shop there is one bathroom. It is shared by all electricians, and therefore it has a lock on the door because Diana Lucas (Brien) had to use it. But sometimes someone might not realize that it was used jointly by both male and female members of the Power Plant family, and they might not lock the door. So, on occasion, Dee would go into the bathroom only to find that it was already occupied.
Once she entered the bathroom and found that someone was in the stall. She waited around for a while and asked me to go check it out because the guy was taking quite a long time and what at first was only a minor inconvenience was becoming higher priority. So, I entered there bathroom and sure enough. The stall was closed and there was a pair of boots easily visible under the stall where someone sat taking their own sweet time.
Dee finally figured that it wasn’t worth the wait and walked across the T-G floor to the maintenance shop to the nearest women’s restroom. After a while someone else remarked that someone was in the bathroom and had been in there a long time. At that point, it became obvious that either someone had died while sitting on his thinkin’ chair, or something else was definitely amiss.
So, one of the electricians decided to see if everything was all right. That was when they peered into the stall to find that there was only a pair of boots sitting all by themselves in the stall. It turned out that O D McGaha had put them there. He locked the stall, then climbed out under the stall and left them there. — It was a pretty good joke. It had half the shop concerned about the mysterious stranger in the stall.
Soon after this episode, a new sign was placed on the bathroom door:
Other little jokes like that were played on individuals throughout the 20 years that I worked at the plant. One small one that is a typical example of many was when Mickey Postman drove to work one morning with a brand new motorcycle. He was really proud of the new machine. Well. Mickey’s nickname at the time was “Pup”.
Mickey had two main reasons why he was a prime target for having jokes played on him. First, he took the jokes pretty well, because he would have a definite reaction. Sometimes good. Sometimes not so. The second reason was that he was red-headed. That meant that when he realized that a joke was being played on him, his face would turn as red as his hair. Everyone witnessing this couldn’t help but smile.
Mickey had worked his way into the maintenance shop from a janitor as I had, though he missed the labor crew (I believe) because it hadn’t been dreamed up by Ray Butler yet. He and I were practically the same age. He is 7 months older than I am. So, I always felt like, “but for the grace of God go I”. No. I don’t really mean it. I care a lot for Mickey and I never personally considered him as a candidate for jokes. I guess it was because he already had a cohort of Power Plant Men willing to play that part.
So, anyway. Mickey had this shiny new motorcycle parked out in the parking lot all day, so it was inevitable that at least one of the many Power Plant Men that had been assigned to the “Play a Joke on Mickey” detail, would happen to pass by the motorcycle in the parking lot. One of them would have felt obligated to reach down and turn the gas valve off.
The word had gone out throughout the plant that the valve had been closed on Mickey’s motorcycle so that we were all to expect that about the time that Mickey hit the bridge over the discharge on the way out the gate, his motorcycle would run out of fuel and die. It’s times like this that you never forget. A simple joke. A couple hundred Power Plant men all chuckling as they drove across the discharge bridge grinning at Mickey trying to restart his brand new motorcycle that had died perfectly positioned midway across the bridge. His face beaming as red as his hair!
I won’t go into the Wedding present that was given to Mickey Postman the day before his wedding. I intended this post to be only about petty or “minor” jokes. That one was a doozy. Actually. I will never post anything about it, other than to say that I wouldn’t ever say anything about how the machinist’s blue dye was applied.
Machinist’s Blue Dye, or Layout fluid is used when honing down a surface to make sure it is flat. There are other uses for it, but that is the one I am most familiar with. I wonder how that blue color looked along with Mickey’s red face…
Here are examples of two small jokes that took a lot of preparation.
The first one involved Howard Chumbley’s chair. Howard was a foreman in the electric shop. One of the nicest Power Plant Men in all of God’s creation. He was shorter than most taller people. And he was particular about how high his chair was adjusted. Being particular about anything automatically meant that you were a prime target for a joke dealing with whatever you were particular about.
Back then (1984), the height of an office chair was adjusted by turning it upside down and spinning the wheel bracket around to screw in or out the shaft.
So, Charles and I would rotate the bottom of the wheels around 1/4 turn each day. That meant just moving the wheels around to one set of wheels. Not very much. Every week the bracket would only be turned about 1 time, especially given that we wouldn’t remember to do it every day.
Eventually, after 5 or 6 weeks, Howard would go to sit down in his chair and realize that it was lower than he would like it to be. So, he would turn it over and lay the seat on his desk and spin the wheel bracket around a few times. Then test it and do it again until it was just the right height. Howard probably never thought about why every month and a half or so, his chair would be too short and he would end up turning it over and adjusting it back up.
This was a joke that Howard never knew was being played, but every time that chair went upside down, you can bet that Charles and I were grinning from ear-to-ear to have been there to watch it.
Ok. the last story has to be about Gene Day. After all. There was no one that I loved playing jokes on more than Gene Day. Actually, half of them, Gene probably never knew had been jokes. I have written two posts about playing jokes on Gene Day. One of them was just about one joke. See “Psychological Profile of a Control Room Operator” and “Power Plant Humor and Joking with Gene Day“.
So, this particular week, I noticed that Gene Day was the auxiliary operator for Unit 1 Boiler. That meant that at least once each shift he was going to walk through the Unit 1 Precipitator Control Room that housed the controls for the 84 transformers on the precipitator roof.
So, I decided, this was a perfect opportunity to play a petty joke on Gene Day. I took an Eeprom chip that was used to hold the control program for a Precipitator control cabinet, and proceeded to rewrite the program.
I found the code in the assembly language code that sent the message to the display when there was an overcurrent trip. That is, when the cabinet trips, the little LCD display would say: “Overcurrent Trip”. I rewrote the code to say: “Gene Day Trip”. This meant finding the code string: 4F:76:65:72:63:75:72:72:65:6E:74:20:54:72:69:70 and replacing it with: 47:65:6E:65:20:44:61:79:20:54:72:69:70:20:20:20. I wrote the program for a specific cabinet in the middle of the precipitator that I could trip without causing an issue in the general operation of the precipitator.
Then I took the chip to the Precipitator Control room and replaced the control chip for that cabinet and left it running. I had seen Gene Day on his way to the Precipitator Control room the day before, so I had a pretty good idea what time he would be passing through. Because no matter how lazy Gene Day was, he was always consistent. (Gene you know I’m kidding…. right?)
Anyway. I spied Gene leaving the control room around the time I expected, so I made haste to the Precip. Control Room and with my screwdriver, after opening the cabinet, I reached down to the tripping mechanism for an overcurrent trip and I tripped the cabinet. Then leaving from the opposite direction that Gene would be arriving, I slipped out of the Precip Control Room and headed for the plant control room to see Gene’s reaction when he arrived.
About the time I was going around the corner in the breezeway toward the Unit 1 elevator, I saw that Gene had already exited the precip. area, so when I entered the T-G basement I quickly called Gene on the gray phone. Gene turned around and went back in the Precip switchgear (which was just below the control cabinets).
When Gene answered the phone I told him that I was looking at the Precipitator controls in the control room and I saw that one of the cabinets had tripped and I was wondering if he had just been out there because the error indicated something very strange. He said he had just been in there and hadn’t noticed that a cabinet had tripped.
So, I asked him if he could look again, it was 1D8. I needed to know what the cabinet display said had happened because it looked like Gene had done something to it. He told me he hadn’t touched anything, but he would go look. — of course, when went to look at it, the display showed: “Gene Day Trip”.
So, I was sitting at the precipitator computer for Unit 1 when Gene Day arrived in the Control room. As was typical with Gene Day, my head began to waiver and my eyes began to blur as Gene had grabbed me by the throat and was shaking me back and forth. My eyes may have been blurry, and I know that I was acting totally surprised as if I didn’t know what had happened, but you can believe that inside I was grinning ear-to-ear!
Comment from original post:
September 21, 2013:
Folks will go to elaborate lengths and great effort to perform jokes like these on fellow workers while feeling put-upon and resentful at something half the trouble requested done by the boss… We are a funny species!
More comments from the last repost:
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“Folks will go to elaborate lengths and great effort to perform jokes like these on fellow workers while feeling put-upon and resentful at something half the trouble requested done by the boss… We are a funny species!” Keeps it entertaining, right? 🙂
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I’ve been following your blog, and in the early a.m. after I’ve gotten the coffee started and my husbands lunch prepared and breakfast fixed, then I sit down to relax and I read your stories, I start laughing, sometimes really hard, and my husband looks at me like I’ve fallen off my rocker!!! What a good way to wake up in the mornings. Thank you for sharing. May God bless you today!
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Cool stories. Workplaces should be like this. I think this is something that is lost on people these days, that you need to laugh.
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I love these stories!
OK Kevin – how could you remember those lines of Eeprom code from 30 years ago?
Also, I know somebody is playing a joke on me (like what you did to Howard Chumbley). My bathroom scales are going up about 1 pound every week. Can’t figure out who’s responsible yet 😦-
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The code is easy to remember: “Overcurrent trip” is translated into ASCII numbers. Where a capital A is 65 and a small A is 97 and then just count up from there. So, the capital O is the ASCII number 79 which when converted to a Hexidecimal number is 4F (16 goes into 79 4 times, with 15 left over. An F represents the number 15). So, “Overcurrenct trip” becomes: 4F:76:65:72:63:75:72:72:65:6E:74:20:54:72:69:70. “Gene Day Trip” is three characters shorter than Overcurrent trip, so, I had to add extra spaces at the end, which are the three “20”s (an ASCII number of 32) on the end of 47:65:6E:65:20:44:61:79:20:54:72:69:70:20:20:20. in order to keep the addresses on the chip consistent.
Another note is that each two digit Hexidecimal code is equal to 8 bits which is a byte. You can determine what each byte is by taking each digit of the Hex number and translating it into 4 binary digits. So… 1 is 0001, 2 is 0010, 3 is 0011, 4 is 0100, 5 is 0101, 6 is 0110, 7 is 0111, 8 is 1000, 9 is 1001, A is 1010, B is 1011, C is 1100, D is 1101, E is 1110, F is 1111
So, the Hex number for a Capital O is 4F, and that indicates an 8 bit byte of: 01001111
And that’s how computers interpret the world. Zeroes and One’s. Or On and Off. So, if there is voltage on the first bit it is a 1 if the voltage is missing, it is a 0.
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So funny! We used to have fun like this on the volunteer fire department. Always makes the tough stuff better when you can laugh together.
Runaway Fire Hydrant Leaves Power Plant in the Dark
Originally posted May 17, 2014:
Don’t believe it when the Electric Company tells you that the reason your town lost electricity for an hour was because a squirrel climbed onto a transformer and shorted it out. The real reason just may be more bizarre than that and the company doesn’t want you to know all the different creative ways that power can be shut off. This is a tale of just one of those ways. So, get out your pencil and paper and take notes.
One spring day in 1993 while sitting at the Precipitator computer for Unit one at the Coal-fired Power Plant in North Central Oklahoma, while I was checking the controls to make sure all the cabinets were operating correctly, suddenly there was a distant boom, and the lights in the control room went out. The computer stayed on because it was connected to an electric panel called the VSP or Vital Services Panel, which in turn was supplied by the UPS system (Uninterruptible Power Supply). That was one of those moments where you may pause for a moment to make sure you aren’t still at home dreaming before you fly into a panic.
The Precipitator cabinets all indicated on the computer that they had just shutdown. I rose from the chair and walked around to the front of the Alarm Panel for Unit one, and found that the fluorescent lights were only out on Unit 1. The lights were still on for Unit 2. The Control Panel was lit up like a Christmas Tree with Green, Red, Blue and Yellow Lights. The Alarm Printer was spewing out paper at high speed. As the large sheets of paper were pouring out onto the floor, I watched as Pat Quiring and other brave Power Plant Control Room operators were scurrying back and forth turning switch handles, pushing buttons, and checking pressure gauges.
Just this site alone gave me confidence that everything was going to be all right. These Control Room operators were all well trained for emergencies just like this, and each person knew what their job was. No one was panicking. Everyone was concentrating on the task at hand.
Someone told me that we lost Unit 1, and the Auxiliary Power to Unit 1 at the same time. So, Unit 1 was dead in the water. This meant, no fans, no pumps, no lights, no vending machines, no cold water at the water fountain and most importantly, no hot coffee!!! I could hear steam valves on the T-G floor banging open and the loud sound of steam escaping.
I turned quickly to go to the electric shop to see what I could do there in case I was needed. I bolted out the door and down the six flights of stairs to the Turbine-Generator (T-G) basement. Exiting the stairway, and entering the T-G basement the sound was deafening. I grabbed the earplugs that were dangling around my neck and crammed them into my ears. Steam was pouring out of various pop-off valves. I ducked into the electric shop where across the room Andy Tubbs, one of the electric foreman was pulling large sheets of electric blueprints from the print cabinet and laying them across the work table that doubled as the lunch table.
When I asked Andy what happened, I learned that somehow when a crew was flushing out a fire hydrant the water somehow shot up and into the bus work in the Auxiliary Substation (that supplies backup power to the Power Plant) and it shorted out the 189,000 volt substation directly to ground. When that happened it tripped unit 1 and the auxiliary substation at the same time leaving it without power.
I will explain how a fire hydrant could possibly spray the bus work in a substation in a little while, but first let me tell you what this meant at the moment to not have any power for a Power Plant Boiler and Turbine Generator that has just tripped when it was at full load which was around 515 Megawatts of power at the time.
Normally when a unit trips, the boiler cools down as the large Force Draft (FD) Fans blow air through the boiler while the even larger Induced Draft (ID) fans suck the air from the boiler on the other end and blow the hot air up the smoke stack. This causes the steam in the boiler tubes to condense back into water. Steam valves open on the boiler that allow excessive steam to escape.
When the boiler is running there is a large orange fireball hovering in space in the middle of the boiler. The boiler water is being circulated through the boiler and the Boiler Feed Pump Turbines are pumping steam back and forth between the turbine generator and the boiler reheating the steam until every bit of heat from the boiler that can be safely harnessed is used.
When all this stop suddenly, then it is important that the large fans keep running to cool down the steam, since it is no longer losing energy in the generator as it was when it was busy supplying electricity to 1/2 million people in Oklahoma City. The power is fed to the fans from the Auxiliary substation located right outside the Main Switchgear where all the breakers reside that supply the power to the fans. Unfortunately, in this case, the Auxiliary substation was shutdown as well, leaving the boiler without any fans.
Without fans for cooling, and pumps to circulate the water, the walls of the boiler began heating up to dangerous temperatures. Steam was whistling out of pop off valves, but if the steam drum on the top of the boiler were to run dry, then the entire boiler structure could be compromised and begin melting down. — So, this was serious. Something had to be done right away. It wouldn’t be as bad as the China Syndrome since we were burning coal instead of nuclear power, but it would have caused a lot of damage nonetheless.

From the movie “The China Syndrome” where a similar emergency existed only in the movie, it was a Nuclear Plant
I have a side story about this picture, but I think I’ll save it for another post because I don’t want to digress from the main story at this point (Ok. Let me just say “Jack Maloy and Merl Wright” for those who can’t wait) See the post: “Power Plant Conspiracy Theory“.
With the prospect that the boiler might melt to the ground in a pile of rubble, it would seem that the main priority was to turn the Auxiliary Substation back on so the fans could be turned back on and prevent the boiler from collapsing. So, we walked out to the substation and looked at the switches that would have to be operated in order to first power up the main bus and then to close to supply power to the two big transformers and the six smaller transformers that supplied the Unit 1 Main Switchgear.
While inspecting the switches where the electricity had gone to ground we found that one of the main insulators was cracked.
Since this insulator was cracked, we didn’t really want to operate the switch to test if another 189,000 volts would go straight to ground again, especially since one of us would be standing right underneath it cranking the switch. So, we went back to the shop to find an alternative.
By this time the Plant Manager, Ron Kilman arrived in the shop, and understanding the urgency to find a solution asked us what were the alternatives. He was relying on our expertise to make the decision.
The other solution would be to cut the power over from Unit 2 which was still humming away pushing electricity to Oklahoma City out of the 345,000 volt substation. The cut over would be very simple because the switchgear was designed with this in mind. We analyzed the power rating on the auxiliary transformers on Unit 2 and thought that we might be cutting it close to have them running both sets of fans at the same time, especially since the full load amps of a huge fan starting up was about 10 times the normal rate.
The transformer was rated to handle the load, but consider this. What if this caused Unit 2 to trip as well. With the Auxiliary substation offline, if Unit 2 tripped, we would be in twice the amount of trouble we were currently in. What a day it would have been if that had happened and two 250 foot boilers had come crashing to the ground in a pile of rubble. After reading the power ratings on the auxiliary transformers I was thinking, “Yeah, let’s do it! These transformers can handle it.” Andy was not so eager.
So, we were left with one alternative. That was to shut the switch in the Auxiliary substation that had the cracked insulator and take our chances that it wasn’t going to short to ground and blow up over our heads. I think I was eager to close the switch for Andy, but if I remember correctly, he didn’t want me to be the one to suffer the consequences and decided to close the switch himself. Needless to say. Andy closed the switch, and nothing blew up.
As soon as the power was restored to the switchgear, the fans were powered up and the temperature in the boiler was quickly reduced. The coffee pot in the Electric Shop began heating the coffee again. The power plant was saved from a major catastrophe. That was delayed for another day… of which I will talk about later (see the post “Destruction of a Power Plant God).”
So, how exactly does a fire hydrant shoot water up into the bus work of a substation like the picture of the switch directly above? The culprit fire hydrant wasn’t in the substation, it sat alongside it outside the fence a good 50 feet from the high voltage switch. No hose was attached to the fire hydrant. It was only being flushed out as part of a yearly activity to go around and make sure the fire hydrants are all operating correctly.
Here is the story about how the squirrel climbed into the transformer this time….
George Alley, Dale Mitchell and Mickey Postman were going around to the 30,000 fire hydrants on the plant ground (ok. maybe not that many, but we did have a lot of them), and they were opening up the valves and flushing them out. That means, they were letting them run for a while to clear them out from any contaminates that may have built up over the year of not being used.
Throughout their adventure they had opened a multitude of Hydrants situated out in the fields along the long belt conveyor from the coalyard and around the two one-million gallon #2 Diesel tanks.
The brave Power Plant Men, learned that when opening a fire hydrant wide open in the middle of field had unintended consequences. It tended to wash out the ground in front of the flow of the water shooting out of the hydrant. So the team of experts devised a plan to place a board in front of the hydrant when it would be in danger of tearing a hole in the terrain. The board would divert the water into the air where it would fan out and not cause damage to the surrounding area.
This was working fine, and when they arrived at the fire hydrant next to the substation, since the stream from the hydrant was pointing directly into the substation (hmm. a design flaw, I think), they decided to prop the board up against the fence to keep from washing away the gravel in the substation. Well. When a fire hydrant is opened that hasn’t been used for a year, the first flow of water to shoot out is dark brown.
You may think that this is because the water has somehow become dirty over the past year, but that isn’t quite the case. What has happened is that the pipe has been rusting little by little and the water has become saturated with the rust. So, the water shooting out of the hydrant was full of rust (hence the need to flush them out).
Well. Rust is made of metal. Metal is conductive, especially when it is mixed with water. When the water hit the board, it was deflected into the air and happened to direct itself directly into the high voltage switch in the substation. This caused a circuit to the ground which, once it created an arc pumped all the electricity directly into the ground.
Normally when something like this happens it doesn’t trip the Main Power Transformer to a Power Plant.
This time it did. I know there was a few heads scratching trying to figure it out. I think I figured out what happened a little while later. You see… here is the rest of the story….
Once the unit was back online and the emergency was over, someone finally noticed that the telephone system couldn’t call outside of the plant. Well. I was the main telephone person at the time, so the control room called me and asked me to look into the problem.
I checked the telephone computer and it was up and running just fine. Internal calls could be made. Only any call outside just concluded with a funny humming sound. After checking the circuit in the Logic Room next to the Rolm Telephone Computer I headed for…. guess where….. the Main Switchgear….
In the middle of the main switchgear in the back of the room right next to the Auxiliary Substation beyond the back wall, the outside telephone line came into the plant. The first thing it did was go through a special Telephone Surge Protector.
In this picture above, the silver circular buttons on the left side are really an old style surge protector. whenever there was a power surge, the carbon connection in the surge protector would quickly melt causing the circuit to go straight to ground. Thus protecting the rest of the telephone circuit. So, if some kid in their house decides to connect the 120 volts circuit to the telephone for fun to see what would happen, this circuit would protect the rest of the phone circuits. Keep in mind that this was during the early 1990 when “Surge Protection” still was basically all “mechanical”.
Anyway, when I arrived at this panel and I checked the surge protector to the main line going out of the plant, guess what I found…. Yep. Shorted to ground. Luckily there were some spares that were not wired to anything in the panel and I was able to swap them out for the ones that had been destroyed. — These were a one time use. Which meant, if they ever had to short to ground, they had to be replaced.
Ok. Fine. After a little while, we were able to call back out of the plant, though there was still some residual noise on the line. It was like this… when you called out of the plant, the person on the other end sounded like they were buried in a grave somewhere and they were trying to talk to someone living just like in an episode of the Twilight Episode where a phone line landed on a grave and the dead person tried to call his long lost love from the past.
I didn’t give it much thought other than that I figured the 189,000 volt arc to ground must have shorted out the telephone line since the phone line ran directly under the auxiliary substation ground grid.
It wasn’t until the next morning when the Southwestern Bell repairman showed up at the plant. I knew him well, since he had been working on our phone lines since before the AT&T breakup in 1984. When I met him in the front of the electric shop, he said that he needed to check our telephone circuits. I told him that I knew that we had a problem because we had a high voltage short to ground yesterday and I found our surge protectors melted away.
He explained to me that not only was our circuit affected, but that every relay house from here to Ponca City was blown out. That’s when I realized that the problem was the reverse of the usual situation. What had happened was that the Ground Grid in the substation and the surrounding area (including the Unit 1 Main Power Transformer) had become hot. What do you do when the ground grid becomes charged?
The Ground Grid is what is supposed to protect you when a surge happens, but what happens when the ground grid itself is the problem? In this case, when the high voltage line about 60 feet from the telephone cable surge protector, arced to ground, it fed a tremendous amount of power back through the ground grid. when equipment detected the surge in voltage, they automatically defaulted their circuits to ground. That’s why the telephone circuit died. That’s what tripped the Main Power Transformer.
When the telephone circuit detected the high voltage surge, it shorted to ground (which was the problem), causing the high voltage to feed directly into the phone line and down the line to the next Southwestern Bell relay switch, which also defaulted to ground, trying to bleed off the surge as it went from relay switch to switch until enough of the power was able to be diverted to ground.
That day sure turned out to be a learning experience. I learned that when all the lights go out in the control room, that it is almost assured that the coffee pot in the electric shop is going to stop working. I also learned that in order to coax the plant manager to the electric shop, a major electrical tragedy is one good way. I learned that when shooting rusty water into the air don’t point it at a high voltage auxiliary substation switch. — I’m sure Mickey Postman learned that lesson too. I also learned that just like in Star Trek… whenever there is a dangerous job to do, the Captain is always the one that wants to do it. Does that make sense? Send a Peon like me in there…
I also learned something else about Power Plant Men…. You see…. People like Dale Mitchell, George Alley and Mickey Postman all are examples of incredibly wonderful Power Plant Men. When they were out there doing their duty and something tragic like this, all the Power Plant Men felt their pain. They knew that they all felt guilty for tripping the unit. It didn’t matter that a million dollars every so many minutes was walking out the door in revenue. The only thing that mattered was that these three men were safe.
Since I have left the Power Plant, I have found that the idea that the employee is the greatest asset that a company can possess is not a universal idea. You see, there was never the thought that any of these people should be fired for their mistake. On the contrary. The true Power Plant Men did whatever they could to let them know that they knew exactly how they felt. It could have happened to any of them.
Besides the friendship between Power Plant Men, one of the things I miss most about working at the Power Plant is that the employees are held in high esteem as a real asset to the company. Many could learn from their example.
Comments from the Original post
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That was an exciting day! Another great story. Thanks for the memories.
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I like the mix of storytelling and information sharing you deliver here. Thanks again
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Aug 8, 2011 I lost all reserve in and lost both units in 2 separate storms and A1 would not start for a few minutes and A2 was leaking antifreeze terribly not a scratch and back online in 34 hours both units and no one ever asked me one question even with a Safety Dept not one question asked of me the SS on duty. Not many men on the planet have ever experienced an uncontrolled total plant outage- you would of thought a learning opportunity would of took place. Feb 2011 worst winter temps in years 50 Units or more tripped in Texas let alone the trusty units of Redbud and McClain were fighting Sooner rolled right along with storm warnings for two weeks ahead – the ICS still went to Detroit for just tours of other facilities once again the fall guy Tarver McArthur stood alone. I had authored a Freeze Protection Plan for the plant and that seemed to save the day and explain to the regulatory bodies how we were online and everyone else in Texas was off and enjoying rolling blackouts in a terrible winter weather situation not to mention our powers that be were all stranded in Detroit and very few people could get to the plant without getting stuck trying to get there as well – but a few health heart issues later I am still here to tell about it all you would think folks would want to take advantage of someone that had went through the fire and Ice but thats ok I want them someday distant to get all the credit they deserve when the trumpets sound as that is truly what matters most. DT
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Great story, and yes, you took exactly the proper lesson from it, and it is too bad that many of our bosses haven’t learned it.
And yup, I’ve buried a lot of electrocuted squirrels over the years.
Petty Power Plant Jokes Played on Prominent Power Plant Men
Originally posted September 13, 2013:
Of the 1,500 jokes played on Power Plant Men while I was working at the Coal-fired Power Plant in North Central Oklahoma, I can only remember a handful of the smaller ones. There are some I’m saving for later topics. Sometimes it was the smallest jokes that spoke the loudest. Especially when great care was taken to play the joke just right.
I think it was the idea that someone thought enough of you to spend a great deal of time setting up a joke just for the one little moment that the person finally realizes that they have been played. It’s when that smile comes across their face that all that work pays off. The realization that someone else would spend so much time just to make you smile was a good indication that they really did care about you.
In the post called, “Why Stanley Elmore and Other Power Plant Questions” I told a story about when I was a janitor in the electric shop and one of the electricians Andy Tubbs had been playing jokes on me while I was cleaning the bathroom. The funniest one was when I had turned around for a moment and when I went to go grab the dust mop, the handle to the mop was missing, while the dust mop was just sitting there on the floor.
Charles Foster, my electric foremen had told me of a time when he played a joke on a welder in the welding shop that was welding away on something. The power to the welding machine was around the corner. Charles picked up the cord for the welder and kinked it like you would kink a water hose to stop the water from flowing. When he kinked it, the welding machine stopped working.
The welder looked at the machine to find that the power was off. Then he looked over and saw that Charles was standing about 40 feet away grinning at him holding the kinked cable. About that time, Charles straightened out the cable and the welding machine turned back on. The welder spun around to find the welding machine humming away. He looked back at Charles who kinked the cable again and the welding machine again shut off.
Amazed, the welder said something like, “I didn’t know you could do that!” Charles shrugged, dropped the cable and walked off. Unbeknownst to the welder, as Charles left, he met up with the other electrician that had been opening an closing the electric disconnect where the welding machine received its power. Leaving the welder unaware.
In the electric shop there is one bathroom. It is shared by all electricians, and therefore it has a lock on the door because Diana Lucas (Brien) had to use it. But sometimes someone might not realize that it was used jointly by both male and female members of the Power Plant family, and they might not lock the door. So, on occasion, Dee would go into the bathroom only to find that it was already occupied.
Once she entered the bathroom and found that someone was in the stall. She waited around for a while and asked me to go check it out because the guy was taking quite a long time and what at first was only a minor inconvenience was becoming higher priority. So, I entered there bathroom and sure enough. The stall was closed and there was a pair of boots easily visible under the stall where someone sat taking their own sweet time.
Dee finally figured that it wasn’t worth the wait and walked across the T-G floor to the maintenance shop to the nearest women’s restroom. After a while someone else remarked that someone was in the bathroom and had been in there a long time. At that point, it became obvious that either someone had died while sitting on his thinkin’ chair, or something else was definitely amiss.
So, one of the electricians decided to see if everything was all right. That was when they peered into the stall to find that there was only a pair of boots sitting all by themselves in the stall. It turned out that O D McGaha had put them there. He locked the stall, then climbed out under the stall and left them there. — It was a pretty good joke. It had half the shop concerned about the mysterious stranger in the stall.
Soon after this episode, a new sign was placed on the bathroom door:
Other little jokes like that were played on individuals throughout the 20 years that I worked at the plant. One small one that is a typical example of many was when Mickey Postman drove to work one morning with a brand new motorcycle. He was really proud of the new machine. Well. Mickey’s nickname at the time was “Pup”.
Mickey had two main reasons why he was a prime target for having jokes played on him. First, he took the jokes pretty well, because he would have a definite reaction. Sometimes good. Sometimes not so. The second reason was that he was red-headed. That meant that when he realized that a joke was being played on him, his face would turn as red as his hair. Everyone witnessing this couldn’t help but smile.
Mickey had worked his way into the maintenance shop from a janitor as I had, though he missed the labor crew (I believe) because it hadn’t been dreamed up by Ray Butler yet. He and I were practically the same age. He is 7 months older than I am. So, I always felt like, “but for the grace of God go I”. No. I don’t really mean it. I care a lot for Mickey and I never personally considered him as a candidate for jokes. I guess it was because he already had a cohort of Power Plant Men willing to play that part.
So, anyway. Mickey had this shiny new motorcycle parked out in the parking lot all day, so it was inevitable that at least one of the many Power Plant Men that had been assigned to the “Play a Joke on Mickey” detail, would happen to pass by the motorcycle in the parking lot. One of them would have felt obligated to reach down and turn the gas valve off.
The word had gone out throughout the plant that the valve had been closed on Mickey’s motorcycle so that we were all to expect that about the time that Mickey hit the bridge over the discharge on the way out the gate, his motorcycle would run out of fuel and die. It’s times like this that you never forget. A simple joke. A couple hundred Power Plant men all chuckling as they drove across the discharge bridge grinning at Mickey trying to restart his brand new motorcycle that had died perfectly positioned midway across the bridge. His face beaming as red as his hair!
I won’t go into the Wedding present that was given to Mickey Postman the day before his wedding. I intended this post to be only about petty or “minor” jokes. That one was a doozy. Actually. I will never post anything about it, other than to say that I wouldn’t ever say anything about how the machinist’s blue dye was applied.
Machinist’s Blue Dye, or Layout fluid is used when honing down a surface to make sure it is flat. There are other uses for it, but that is the one I am most familiar with. I wonder how that blue color looked along with Mickey’s red face…
Here are examples of two small jokes that took a lot of preparation.
The first one involved Howard Chumbley’s chair. Howard was a foreman in the electric shop. One of the nicest Power Plant Men in all of God’s creation. He was shorter than most taller people. And he was particular about how high his chair was adjusted. Being particular about anything automatically meant that you were a prime target for a joke dealing with whatever you were particular about.
Back then (1984), the height of an office chair was adjusted by turning it upside down and spinning the wheel bracket around to screw in or out the shaft.
So, Charles and I would rotate the bottom of the wheels around 1/4 turn each day. That meant just moving the wheels around to one set of wheels. Not very much. Every week the bracket would only be turned about 1 time, especially given that we wouldn’t remember to do it every day.
Eventually, after 5 or 6 weeks, Howard would go to sit down in his chair and realize that it was lower than he would like it to be. So, he would turn it over on and lay the seat on his desk and spin the wheel bracket around a few times. Then test it and do it again until it was just the right height. Howard probably never thought about why every month and a half or so, his chair would be too short and he would end up turning it over and adjusting it back up.
This was a joke that Howard never knew was being played, but every time that chair went upside down, you can bet that Charles and I were grinning from ear-to-ear to have been there to watch it.
Ok. the last story has to be about Gene Day. After all. There was no one that I loved playing jokes on more than Gene Day. Actually, half of them, Gene probably never knew had been jokes. I have written two posts about playing jokes on Gene Day. One of them was just about one joke. See “Psychological Profile of a Control Room Operator” and “Power Plant Humor and Joking with Gene Day“.
So, this particular week, I noticed that Gene Day was the auxiliary operator for Unit 1 Boiler. That meant that at least once each shift he was going to walk through the Unit 1 Precipitator Control Room that housed the controls for the 84 transformers on the precipitator roof.
So, I decided, this was a perfect opportunity to play a petty joke on Gene Day. I took an Eeprom chip that was used to hold the control program for a Precipitator control cabinet, and proceeded to rewrite the program.
I found the code in the assembly language code that sent the message to the display when there was an overcurrent trip. That is, when the cabinet trips, the little LCD display would say: “Overcurrent Trip”. I rewrote the code to say: “Gene Day Trip”. This meant finding the code string: 4F:76:65:72:63:75:72:72:65:6E:74:20:54:72:69:70 and replacing it with: 47:65:6E:65:20:44:61:79:20:54:72:69:70:20:20:20. I wrote the program for a specific cabinet in the middle of the precipitator that I could trip without causing an issue in the general operation of the precipitator.
Then I took the chip to the Precipitator Control room and replaced the control chip for that cabinet and left it running. I had seen Gene Day on his way to the Precipitator Control room the day before, so I had a pretty good idea what time he would be passing through. Because no matter how lazy Gene Day was, he was always consistent. (Gene you know I’m kidding…. right?)
Anyway. I spied Gene leaving the control room around the time I expected, so I made haste to the Precip. Control Room and with my screwdriver, after opening the cabinet, I reached down to the tripping mechanism for an overcurrent trip and I tripped the cabinet. Then leaving from the opposite direction that Gene would be arriving, I slipped out of the Precip Control Room and headed for the plant control room to see Gene’s reaction when he arrived.
About the time I was going around the corner in the breezeway toward the Unit 1 elevator, I saw that Gene had already exited the precip. area, so when I entered the T-G basement I quickly called Gene on the gray phone. Gene turned around and went back in the Precip switchgear (which was just below the control cabinets).
When Gene answered the phone I told him that I was looking at the Precipitator controls in the control room and I saw that one of the cabinets had tripped and I was wondering if he had just been out there because the error indicated something very strange. He said he had just been in there and hadn’t noticed that a cabinet had tripped.
So, I asked him if he could look again, it was 1D8. I needed to know what the cabinet display said had happened because it looked like Gene had done something to it. He told me he hadn’t touched anything, but he would go look. — of course, when went to look at it, the display showed: “Gene Day Trip”.
So, I was sitting at the precipitator computer for Unit 1 when Gene Day arrived in the Control room. As was typical with Gene Day, my head began to waiver and my eyes began to blur as Gene had grabbed me by the throat and was shaking me back and forth. My eyes may have been blurry, and I know that I was acting totally surprised as if I didn’t know what had happened, but you can believe that inside I was grinning ear-to-ear!
Comment from original post:
September 21, 2013:
Folks will go to elaborate lengths and great effort to perform jokes like these on fellow workers while feeling put-upon and resentful at something half the trouble requested done by the boss… We are a funny species!
More comments from the last repost:
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“Folks will go to elaborate lengths and great effort to perform jokes like these on fellow workers while feeling put-upon and resentful at something half the trouble requested done by the boss… We are a funny species!” Keeps it entertaining, right? 🙂
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I’ve been following your blog, and in the early a.m. after I’ve gotten the coffee started and my husbands lunch prepared and breakfast fixed, then I sit down to relax and I read your stories, I start laughing, sometimes really hard, and my husband looks at me like I’ve fallen off my rocker!!! What a good way to wake up in the mornings. Thank you for sharing. May God bless you today!
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Cool stories. Workplaces should be like this. I think this is something that is lost on people these days, that you need to laugh.
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I love these stories!
OK Kevin – how could you remember those lines of Eeprom code from 30 years ago?
Also, I know somebody is playing a joke on me (like what you did to Howard Chumbley). My bathroom scales are going up about 1 pound every week. Can’t figure out who’s responsible yet 😦-
The code is easy to remember: “Overcurrent trip” is translated into ASCII numbers. Where a capital A is 65 and a small A is 97 and then just count up from there. So, the capital O is the ASCII number 79 which when converted to a Hexidecimal number is 4F (16 goes into 79 4 times, with 15 left over. An F represents the number 15). So, “Overcurrenct trip” becomes: 4F:76:65:72:63:75:72:72:65:6E:74:20:54:72:69:70. “Gene Day Trip” is three characters shorter than Overcurrent trip, so, I had to add extra spaces at the end, which are the three “20”s (an ASCII number of 32) on the end of 47:65:6E:65:20:44:61:79:20:54:72:69:70:20:20:20. in order to keep the addresses on the chip consistent.
Another note is that each two digit Hexidecimal code is equal to 8 bits which is a byte. You can determine what each byte is by taking each digit of the Hex number and translating it into 4 binary digits. So… 1 is 0001, 2 is 0010, 3 is 0011, 4 is 0100, 5 is 0101, 6 is 0110, 7 is 0111, 8 is 1000, 9 is 1001, A is 1010, B is 1011, C is 1100, D is 1101, E is 1110, F is 1111
So, the Hex number for a Capital O is 4F, and that indicates an 8 bit byte of: 01001111
And that’s how computers interpret the world. Zeroes and One’s. Or On and Off. So, if there is voltage on the first bit it is a 1 if the voltage is missing, it is a 0.
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So funny! We used to have fun like this on the volunteer fire department. Always makes the tough stuff better when you can laugh together.
Runaway Fire Hydrant Leaves Power Plant in the Dark
Originally posted May 17, 2014:
Don’t believe it when the Electric Company tells you that the reason your town lost electricity for an hour was because a squirrel climbed onto a transformer and shorted it out. The real reason just may be more bizarre than that and the company doesn’t want you to know all the different creative ways that power can be shut off. This is a tale of just one of those ways. So, get out your pencil and paper and take notes.
One spring day in 1993 while sitting at the Precipitator computer for Unit one at the Coal-fired Power Plant in North Central Oklahoma, while I was checking the controls to make sure all the cabinets were operating correctly, suddenly there was a distant boom, and the lights in the control room went out. The computer stayed on because it was connected to an electric panel called the VSP or Vital Services Panel, which in turn was supplied by the UPS system (Uninterruptible Power Supply). That was one of those moments where you may pause for a moment to make sure you aren’t still at home dreaming before you fly into a panic.
The Precipitator cabinets all indicated on the computer that they had just shutdown. I rose from the chair and walked around to the front of the Alarm Panel for Unit one, and found that the fluorescent lights were only out on Unit 1. The lights were still on for Unit 2. The Control Panel was lit up like a Christmas Tree with Green, Red, Blue and Yellow Lights. The Alarm Printer was spewing out paper at high speed. As the large sheets of paper were pouring out onto the floor, I watched as Pat Quiring and other brave Power Plant Control Room operators were scurrying back and forth turning switch handles, pushing buttons, and checking pressure gauges.
Just this site alone gave me confidence that everything was going to be all right. These Control Room operators were all well trained for emergencies just like this, and each person knew what their job was. No one was panicking. Everyone was concentrating on the task at hand.
Someone told me that we lost Unit 1, and the Auxiliary Power to Unit 1 at the same time. So, Unit 1 was dead in the water. This meant, no fans, no pumps, no lights, no vending machines, no cold water at the water fountain and most importantly, no hot coffee!!! I could hear steam valves on the T-G floor banging open and the loud sound of steam escaping.
I turned quickly to go to the electric shop to see what I could do there in case I was needed. I bolted out the door and down the six flights of stairs to the Turbine-Generator (T-G) basement. Exiting the stairway, and entering the T-G basement the sound was deafening. I grabbed the earplugs that were dangling around my neck and crammed them into my ears. Steam was pouring out of various pop-off valves. I ducked into the electric shop where across the room Andy Tubbs, one of the electric foreman was pulling large sheets of electric blueprints from the print cabinet and laying them across the work table that doubled as the lunch table.
When I asked Andy what happened, I learned that somehow when a crew was flushing out a fire hydrant the water somehow shot up and into the bus work in the Auxiliary Substation (that supplies backup power to the Power Plant) and it shorted out the 189,000 volt substation directly to ground. When that happened it tripped unit 1 and the auxiliary substation at the same time leaving it without power.
I will explain how a fire hydrant could possibly spray the bus work in a substation in a little while, but first let me tell you what this meant at the moment to not have any power for a Power Plant Boiler and Turbine Generator that has just tripped when it was at full load which was around 515 Megawatts of power at the time.
Normally when a unit trips, the boiler cools down as the large Force Draft (FD) Fans blow air through the boiler while the even larger Induced Draft (ID) fans suck the air from the boiler on the other end and blow the hot air up the smoke stack. This causes the steam in the boiler tubes to condense back into water. Steam valves open on the boiler that allow excessive steam to escape.
When the boiler is running there is a large orange fireball hovering in space in the middle of the boiler. The boiler water is being circulated through the boiler and the Boiler Feed Pump Turbines are pumping steam back and forth between the turbine generator and the boiler reheating the steam until every bit of heat from the boiler that can be safely harnessed is used.
When all this stop suddenly, then it is important that the large fans keep running to cool down the steam, since it is no longer losing energy in the generator as it was when it was busy supplying electricity to 1/2 million people in Oklahoma City. The power is fed to the fans from the Auxiliary substation located right outside the Main Switchgear where all the breakers reside that supply the power to the fans. Unfortunately, in this case, the Auxiliary substation was shutdown as well, leaving the boiler without any fans.
Without fans for cooling, and pumps to circulate the water, the walls of the boiler began heating up to dangerous temperatures. Steam was whistling out of pop off valves, but if the steam drum on the top of the boiler were to run dry, then the entire boiler structure could be compromised and begin melting down. — So, this was serious. Something had to be done right away. It wouldn’t be as bad as the China Syndrome since we were burning coal instead of nuclear power, but it would have caused a lot of damage nonetheless.

From the movie “The China Syndrome” where a similar emergency existed only in the movie, it was a Nuclear Plant
I have a side story about this picture, but I think I’ll save it for another post because I don’t want to digress from the main story at this point (Ok. Let me just say “Jack Maloy and Merl Wright” for those who can’t wait) See the post: “Power Plant Conspiracy Theory“.
With the prospect that the boiler might melt to the ground in a pile of rubble, it would seem that the main priority was to turn the Auxiliary Substation back on so the fans could be turned back on and prevent the boiler from collapsing. So, we walked out to the substation and looked at the switches that would have to be operated in order to first power up the main bus and then to close to supply power to the two big transformers and the six smaller transformers that supplied the Unit 1 Main Switchgear.
While inspecting the switches where the electricity had gone to ground we found that one of the main insulators was cracked.
Since this insulator was cracked, we didn’t really want to operate the switch to test if another 189,000 volts would go straight to ground again, especially since one of us would be standing right underneath it cranking the switch. So, we went back to the shop to find an alternative.
By this time the Plant Manager, Ron Kilman arrived in the shop, and understanding the urgency to find a solution asked us what were the alternatives. He was relying on our expertise to make the decision.
The other solution would be to cut the power over from Unit 2 which was still humming away pushing electricity to Oklahoma City out of the 345,000 volt substation. The cut over would be very simple because the switchgear was designed with this in mind. We analyzed the power rating on the auxiliary transformers on Unit 2 and thought that we might be cutting it close to have them running both sets of fans at the same time, especially since the full load amps of a huge fan starting up was about 10 times the normal rate.
The transformer was rated to handle the load, but consider this. What if this caused Unit 2 to trip as well. With the Auxiliary substation offline, if Unit 2 tripped, we would be in twice the amount of trouble we were currently in. What a day it would have been if that had happened and two 250 foot boilers had come crashing to the ground in a pile of rubble. After reading the power ratings on the auxiliary transformers I was thinking, “Yeah, let’s do it! These transformers can handle it.” Andy was not so eager.
So, we were left with one alternative. That was to shut the switch in the Auxiliary substation that had the cracked insulator and take our chances that it wasn’t going to short to ground and blow up over our heads. I think I was eager to close the switch for Andy, but if I remember correctly, he didn’t want me to be the one to suffer the consequences and decided to close the switch himself. Needless to say. Andy closed the switch, and nothing blew up.
As soon as the power was restored to the switchgear, the fans were powered up and the temperature in the boiler was quickly reduced. The coffee pot in the Electric Shop began heating the coffee again. The power plant was saved from a major catastrophe. That was delayed for another day… of which I will talk about later (see the post “Destruction of a Power Plant God).”
So, how exactly does a fire hydrant shoot water up into the bus work of a substation like the picture of the switch directly above? The culprit fire hydrant wasn’t in the substation, it sat alongside it outside the fence a good 50 feet from the high voltage switch. No hose was attached to the fire hydrant. It was only being flushed out as part of a yearly activity to go around and make sure the fire hydrants are all operating correctly.
Here is the story about how the squirrel climbed into the transformer this time….
George Alley, Dale Mitchell and Mickey Postman were going around to the 30,000 fire hydrants on the plant ground (ok. maybe not that many, but we did have a lot of them), and they were opening up the valves and flushing them out. That means, they were letting them run for a while to clear them out from any contaminates that may have built up over the year of not being used.
Throughout their adventure they had opened a multitude of Hydrants situated out in the fields along the long belt conveyor from the coalyard and around the two one-million gallon #2 Diesel tanks.
The brave Power Plant Men, learned that when opening a fire hydrant wide open in the middle of field had unintended consequences. It tended to wash out the ground in front of the flow of the water shooting out of the hydrant. So the team of experts devised a plan to place a board in front of the hydrant when it would be in danger of tearing a hole in the terrain. The board would divert the water into the air where it would fan out and not cause damage to the surrounding area.
This was working fine, and when they arrived at the fire hydrant next to the substation, since the stream from the hydrant was pointing directly into the substation (hmm. a design flaw, I think), they decided to prop the board up against the fence to keep from washing away the gravel in the substation. Well. When a fire hydrant is opened that hasn’t been used for a year, the first flow of water to shoot out is dark brown.
You may think that this is because the water has somehow become dirty over the past year, but that isn’t quite the case. What has happened is that the pipe has been rusting little by little and the water has become saturated with the rust. So, the water shooting out of the hydrant was full of rust (hence the need to flush them out).
Well. Rust is made of metal. Metal is conductive, especially when it is mixed with water. When the water hit the board, it was deflected into the air and happened to direct itself directly into the high voltage switch in the substation. This caused a circuit to the ground which, once it created an arc pumped all the electricity directly into the ground.
Normally when something like this happens it doesn’t trip the Main Power Transformer to a Power Plant.
This time it did. I know there was a few heads scratching trying to figure it out. I think I figured out what happened a little while later. You see… here is the rest of the story….
Once the unit was back online and the emergency was over, someone finally noticed that the telephone system couldn’t call outside of the plant. Well. I was the main telephone person at the time, so the control room called me and asked me to look into the problem.
I checked the telephone computer and it was up and running just fine. Internal calls could be made. Only any call outside just concluded with a funny humming sound. After checking the circuit in the Logic Room next to the Rolm Telephone Computer I headed for…. guess where….. the Main Switchgear….
In the middle of the main switchgear in the back of the room right next to the Auxiliary Substation beyond the back wall, the outside telephone line came into the plant. The first thing it did was go through a special Telephone Surge Protector.
In this picture above, the silver circular buttons on the left side are really an old style surge protector. whenever there was a power surge, the carbon connection in the surge protector would quickly melt causing the circuit to go straight to ground. Thus protecting the rest of the telephone circuit. So, if some kid in their house decides to connect the 120 volts circuit to the telephone for fun to see what would happen, this circuit would protect the rest of the phone circuits. Keep in mind that this was during the early 1990 when “Surge Protection” still was basically was all “mechanical”.
Anyway, when I arrived at this panel and I checked the surge protector to the main line going out of the plant, guess what I found…. Yep. Shorted to ground. Luckily there were some spares that were not wired to anything in the panel and I was able to swap them out for the ones that had been destroyed. — These were a one time use. Which meant, if they ever had to short to ground, they had to be replaced.
Ok. Fine. After a little while, we were able to call back out of the plant, though there was still some residual noise on the line. It was like this… when you called out of the plant, the person on the other end sounded like they were buried in a grave somewhere and they were trying to talk to someone living just like in an episode of the Twilight Episode where a phone line landed on a grave and the dead person tried to call his long lost love from the past.
I didn’t give it much thought other than that I figured the 189,000 volt arc to ground must have shorted out the telephone line since the phone line ran directly under the auxiliary substation ground grid.
It wasn’t until the next morning when the Southwestern Bell repairman showed up at the plant. I knew him well, since he had been working on our phone lines since before the AT&T breakup in 1984. When I met him in the front of the electric shop, he said that he needed to check our telephone circuits. I told him that I knew that we had a problem because we had a high voltage short to ground yesterday and I found our surge protectors melted away.
He explained to me that not only was our circuit affected, but that every relay house from here to Ponca City was blown out. That’s when I realized that the problem was the reverse of the usual situation. What had happened was that the Ground Grid in the substation and the surrounding area (including the Unit 1 Main Power Transformer) had become hot. What do you do when the ground grid becomes charged?
The Ground Grid is what is supposed to protect you when a surge happens, but what happens when the ground grid itself is the problem? In this case, when the high voltage line about 60 feet from the telephone cable surge protector, arced to ground, it fed a tremendous amount of power back through the ground grid. when equipment detected the surge in voltage, they automatically defaulted their circuits to ground. That’s why the telephone circuit died. That’s what tripped the Main Power Transformer.
When the telephone circuit detected the high voltage surge, it shorted to ground (which was the problem), causing the high voltage to feed directly into the phone line and down the line to the next Southwestern Bell relay switch, which also defaulted to ground, trying to bleed off the surge as it went from relay switch to switch until enough of the power was able to be diverted to ground.
That day sure turned out to be a learning experience. I learned that when all the lights go out in the control room, that it is almost assured that the coffee pot in the electric shop is going to stop working. I also learned that in order to coax the plant manager to the electric shop, a major electrical tragedy is one good way. I learned that when shooting rusty water into the air don’t point it at a high voltage auxiliary substation switch. — I’m sure Mickey Postman learned that lesson too. I also learned that just like in Star Trek… whenever there is a dangerous job to do, the Captain is always the one that wants to do it. Does that make sense? Send a Peon like me in there…
I also learned something else about Power Plant Men…. You see…. People like Dale Mitchell, George Alley and Mickey Postman all are examples of incredibly wonderful Power Plant Men. When they were out there doing their duty and something tragic like this, all the Power Plant Men felt their pain. They knew that they all felt guilty for tripping the unit. It didn’t matter that a million dollars every so many minutes was walking out the door in revenue. The only thing that mattered was that these three men were safe.
Since I have left the Power Plant, I have found that the idea that the employee is the greatest asset that a company can possess is not a universal idea. You see, there was never the thought that any of these people should be fired for their mistake. On the contrary. The true Power Plant Men did whatever they could to let them know that they knew exactly how they felt. It could have happened to any of them.
Besides the friendship between Power Plant Men, one of the things I miss most about working at the Power Plant is that the employees are held in high esteem as a real asset to the company. Many could learn from their example.
Comments from the Original post
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That was an exciting day! Another great story. Thanks for the memories.
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I like the mix of storytelling and information sharing you deliver here. Thanks again
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Aug 8, 2011 I lost all reserve in and lost both units in 2 separate storms and A1 would not start for a few minutes and A2 was leaking antifreeze terribly not a scratch and back online in 34 hours both units and no one ever asked me one question even with a Safety Dept not one question asked of me the SS on duty. Not many men on the planet have ever experienced an uncontrolled total plant outage- you would of thought a learning opportunity would of took place. Feb 2011 worst winter temps in years 50 Units or more tripped in Texas let alone the trusty units of Redbud and McClain were fighting Sooner rolled right along with storm warnings for two weeks ahead – the ICS still went to Detroit for just tours of other facilities once again the fall guy Tarver McArthur stood alone. I had authored a Freeze Protection Plan for the plant and that seemed to save the day and explain to the regulatory bodies how we were online and everyone else in Texas was off and enjoying rolling blackouts in a terrible winter weather situation not to mention our powers that be were all stranded in Detroit and very few people could get to the plant without getting stuck trying to get there as well – but a few health heart issues later I am still here to tell about it all you would think folks would want to take advantage of someone that had went through the fire and Ice but thats ok I want them someday distant to get all the credit they deserve when the trumpets sound as that is truly what matters most. DT
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Great story, and yes, you took exactly the proper lesson from it, and it is too bad that many of our bosses haven’t learned it.
And yup, I’ve buried a lot of electrocuted squirrels over the years.
Rivers and Rose in the Power Plant Palace
Originally posted January 25, 2013:
When is the appropriate time to call 911? Calling 911 in the Power Plant is when you call the Shift Supervisor to report something important. As Randy Dailey, our Safety Trainer extraordinaire, always taught us, first tap the person on the shoulder and say, “Are you all right?” Then you point you finger at someone and say, “Call 911!” That’s called “Activating the EMS” (Emergency Medical System). Besides medical emergencies, there are other reasons to call the Shift Supervisor.
I learned early on to ‘fess up when you have done something wrong.” People appreciate it when you tell them up front that you goofed. That way the problem can be dealt with directly. Dee Ball was that way. Any time he wrecked a truck, he didn’t hesitate to tell his boss. So, even as a summer help I had developed this philosophy. Never be afraid to expose your blunders. It works out better in the long run.
One example of someone not following this philosoply was Curtis Love. As I mentioned in the post Power Plant Spider Wars and Bugs in the Basement, Curtis didn’t want to tell anyone that he had been bitten by a brown recluse for the third time because he was afraid of losing his job.
His philosophy came back to bite him a year and a half later when he was on the labor crew when he was the designated truck driver. I had moved on to the electric shop by this time.
He was backing up the crew cab around a corner under the Fly Ash hoppers up at the coalyard when the side of the crew cab came into contact with one of those yellow poles designed to protect the structure from rogue vehicles. Unfortunately. This created a dent in the side of the truck.
Curtis, already on probation. worried that he would be fired if he told anyone about this mishap, failed to tell Larry Riley about this incident. Larry, on the other hand, was standing in front of the Coalyard Maintenance shop (the labor crew home), and saw the entire incident. At that moment, he turned to one of the labor crew hands and said, “I hope Curtis comes over here and tells me about that.” Unfortunately, Curtis decided to act as if nothing had happened. This resulted in his termination. As much as I cared about Curtis, I must admit that the Power Plant scene was probably not the best location for his vocation.
I had seen Dee Ball do the same thing over and over again, and he always reported his accidents immediately. He was never punished for an accident, though, for a number of years, he was banned from driving a truck. You can read more about this in the post: Experiencing Maggots, Mud and Motor Vehicles with Dee Ball.
One day during the summer of 1984 just after lunch, 1A PA fan tripped (PA stands for Primary Air). When this happened, number one unit had to lower it’s output from over 500 Megawatts down to around 200. The trip indicator on the 6900 volt breaker said that it had been grounded. Being grounded means that one of the three phases of the motor or cable had made a circuit with the ground (or something that was grounded). The trip circuits shut the fan down so fast that it prevents an explosion and saves the fan from being destroyed.
Diana Lucas (later Diana Brien), Andy Tubbs and I were given the task of finding the ground and seeing what we could do to fix it. We unwired the motor, which was no easy task, because the motor is about the size of a large van, and about 10 times heavier.
So, we spent the rest of the day unwiring the motor (in the rain), and unwiring the cable to the motor from the breaker in the main switchgear and testing both the motor and the cable with various instruments looking for the grounded wire or coil that caused the motor to trip. We used a large “Megger” on the motor. It’s called a Megger because it measures Mega-Ohms. So, it’s technically called a Mega-Ohm meter. Ohms is a measurement of resistance in an electrical circuit. We usually use a small hand cranked megger, that is similar to an old hand crank telephone that generates a high voltage (good for shocking fish in a lake to make them rise to the surface). In the case of the hand cranked Megger, it would generate 1,000 volts.
The Megger this size would have been useless with this large motor. Instead we used one that was electric, and you ran the voltage up over 10,000 volts and watched the mega-ohms over a period of 1/2 hour or so.
For the cables, we hooked up a Hypot (or Hipot). This stands for High Potential. Potential in this case is another word for “Voltage”. It would charge up and then you pressed a button and it would send a high voltage pulse down the cable, and if there is a weak spot in the insulation,The Hypot will find it. So, we hooked a Hypot up to the cable and tried to find the grounded wire. No luck.
After spending 4 hours looking for the grounded cable or motor, we found nothing. We spent another hour and a half putting the motor and the breaker back in service. The Fan was put back into operation and we went home. As I was walking out to the car with Bill Rivers, he told me, “I knew they weren’t going to find anything wrong with that fan.” He had a big grin on his face.
At first I thought he was just making an educated guess as Rivers was apt to do on many occasions (daily). It was raining and I could see where water may have been sucked into the motor or something and had momentarily grounded the motor. Just because we didn’t find anything didn’t mean that the breaker didn’t trip for no reason.
When we were in the car and on our way to Stillwater, Oklahoma with Yvonne Taylor and Rich Litzer, Bill explained that he knew why the motor tripped. He had been walking through the main switchgear with Mike Rose, and Mike, for no apparent reason other than curiosity, had opened up the bottom door to the breaker for 1A PA fan. He looked at it for a moment and then slammed the door shut. When he did this, the breaker tripped.
So, the ground relay happened to be the one that tripped. It might as well been an over-current or a low voltage trip. It just happened to trip the ground trip. Bill said that he told Mike that he should call the Shift Supervisor and let him know so they could restart the motor. Mike on the other hand told Bill that he was already on probation and was afraid of losing his job if he reported that he had slammed the door on the breaker and tripped the fan.
If there was ever a reason to call 911, it was then. All he had to do was tell them, “I accidentally tripped the PA fan when I bumped the breaker cabinet.” They would have told him to reset the flag, and they would have started the fan right back up. No questions asked… I’m sure of it. And they wouldn’t have lost their generating capacity for the remainder of the afternoon and we wouldn’t have spent 4 hours unwiring, testing and rewiring the motor in the rain with a plastic umbrella over our head.
Bill wasn’t about to tell on Mike. If Mike didn’t want to report it, Bill wasn’t going to say anything, and I understand that. I probably would have kept it to myself at the time if I was in Bill’s shoes (I’m just glad I wasn’t because I probably wouldn’t have been able to sleep soundly for the next year). But 30 years later, I might write about it in a Blog. Even though I wouldn’t have looked to Mike to teach me much about being an electrician (he was more of an Air Condition man anyway), I still loved the guy.
Mike died almost two years ago on May 29, 2011. He was from England and had lived in Canada for a time. He used to work on trains. Trains, even though they are diesel, are really electric. The Diesel engine really runs a generator that generates electricity that runs the train. I know that Mike was a good man at heart. He loved his family with all his heart. Here is a picture of the Limey:
Ok. So I know what you are thinking…. There must be a story about myself in here somewhere. Well, you would be right. First of all. I always ‘fessed up to my mistakes, as my current manager at Dell knows well (yes. I still mess up after all these years). I told my current manager the other day that CLM was my middle name. (CLM means “Career Limiting Move”). So here is my power plant “mess up” story (well one of them):
In January 1986, I returned from my Honeymoon with my new wife Kelly when I found that we had hired a new electrician. Gsry Wehunt was replacing Jim Stephenson who had left the plant on February 15, 1985, which is a story all it’s own. We had just started an overhaul on Unit 1.
I remember the first Monday I spent with Gary. It was January 6, 1986 and we were working on cleaning out the exciter house on the end of the main power generator with Diana Brien (formerly Diana Lucas). We were discussing salaries and Gary was surprised to find out that I was making more than he was. Well… I had been an electrician for over 2 years and had been promoted regularly…. so I didn’t think there was anything strange about it, except that I still looked like I was only about 18 years old (even though I was 25) and Gary was about 34. I had already been promoted 4 times and my salary had gone from $7.15 to over $12 an hour.
Anyway, when that first Friday rolled around, Gary and I were assigned to Substation Inspection. Some later time I may go into the details of what “Substation Inspection” entails, but for now, let’s just stick with my “911 call.” It is enough to say that we were in the main plant substation relay house on Friday January 10, 1986 at 9:00 am. One of our jobs was to call other substations and perform a test called a “Transfer Trip and Carrier Test”. We had called Woodring Substation (Woodring is a town in Oklahoma and we had a 345 KV line going there), and I was talking to the man in the substation on the other end of the phone line.
At the same time I was showing Gary just how experienced I was at being an electrician. People had told me that you had to be a plant electrician for 5 years before you really became a “first class” electrician. Well. Here I was at 2 years, and I thought I was so good that I could do anything by now…. — Yeah… right. I told the guy on the other end of the line as I turned a switch…. Amber light… Back to Blue…. and I wrote down the value on the meter (paperwork… oh yes…. it’s that important. Like A-1 sauce).
Then I reached for the second switch. I said, “Carrier test”, then turned the switch. The lights in the relay house went out and we were in the dark. I told the guy on the other end of the line….. “Well. That’s not supposed to happen.” Then as I let go of the switch and it returned to it’s normal position, the lights turned back on. Okay……
I wrote the numbers down from the meter and said goodbye to the other faceless substation man on the other end of the line that I talked to over 100 times, but never met in person. He sounded like a nice guy. Then I headed for the gray phone. I heard the Shift Supervisor paging Leroy Godfrey (The Electrical Supervisor) on line 2 (we had 5 Gray phone lines. The Gray Phone was our PA system).
When I picked up the line I heard Leroy pick up the phone and the Shift Supervisor tell Leroy that we just lost station power in the main substation and it had switched over to Auxiliary power. I immediately jumped in and said, “Jim (for Jim Padgett, the Shift Supervisor), I did that. I was performing a Carrier test with Woodring and the moment I performed the carrier test the lights went out.” Leroy chimed in by saying, “That wouldn’t cause you to lose station power.”
Well, in my ‘inexperienced’ plant electrician way, I responded, “Well. All I know is that when I turned the switch to perform the carrier test, the lights went out, and when I let go of the switch, the lights came back on.” Leroy reiterated, “That wouldn’t cause you to lose station power.” I replied with, “I’m just saying….” and left it at that. I had done my job. They knew I was out here. They knew I had called 911 right away. I explained what I was doing…. they could take it from there.
I had hoped that I had showed Gary upfront that it doesn’t hurt to report your mistakes (even though I hadn’t made one as far as I could tell), but I was 100% sure I had done something to cause the relay house to lose power. Though, I couldn’t figure out why.
After lunch, Bill Bennett, our A foreman came down to the shop to tell me that they figured out how the substation lost station power. He said that a road grader had been grating the road down by the Otoe-Missouri reservation (which is actually called “Windmill road” I guess because there is a windmill down that road somewhere), and had hit an electric pole and knocked it over and had killed the power to the substation.
It turned out that the substation relay house was fed by a substation down that road where we have a radio tower. So, think about this. The exact time that I turned that switch in the substation, a road grater 2 1/2 miles away hits a telephone pole accidentally and knocks it to the ground and kills the power to the substation at the exact same time that I am performing a transfer-trip and Carrier test with Woodring Substation, and the time it takes to switch to auxiliary power is the exact time it took me to let go of the switch.
Don’t tell me that was by accident. I will never believe it. I think it was for the soul purpose of teaching me a useful lesson or two. First….. don’t be afraid to tell someone when you do something wrong. Second…. If you think you have control over the things that happen to you in your life… well, think again…… Third….. God watches you every moment, and if you let him, he will guide you to do the right thing when the time comes.
God bless you all.
COMMENTS FROM THE ORIGINAL POST:
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Monty Hansen January 26, 2013
I had a similar thing happen to me, I was upgrading to shift foreman & system called to remove a tag in the switchyard & put the switch back to auto. The tag on the pistol grip was attached with a plastic zip tie & the previous operator had put it on real tight, as I was wrestling it off with my leatherman, the pliers slipped & I banged my elbow into the control panel, at that very instant there was a loud BANG as several 345 KV breakers opened simultaniously in the swithyard, I had the phone pinched between my shoulder & ear as I was wrestling with this switch & talking to the system control operator, he said a few bad words – gotta go – & hung up. The power plant lost all power & went in the black, I, of course was just sick in the pit of my stomach, after we got power restored, the plant back on etc. I called system back to see if they found the cause & fess up to causing the trip (I figured I must have caused a trip relay to close when I hit the panel) – anyway a crane at a plant down the road had got it’s boom tangled in the power line & went to ground – AT PRECISELY THE INSTANT MY ELBOW SLIPPED & HIT THE PANEL!!
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Ron Kilman January 26, 2013
Some great illustrations of the truth in Proverbs 28:13 “He who conceals his transgressions will not prosper, But he who confesses and forsakes them will find compassion”.
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justturnright January 28, 2013
CLM: I can relate.
My first boss 30 years ago once told me he was going to officially nickname me “I’m sorry” (and make me wear it for a name badge) if I said it one more time.
Hey, there’s worse things.
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Roomy January 29, 2013
I had not thought about Mike Rose in years. He was a good guy to work with, now Rivers was a different story!!!
Sub checks, I used to love to do sub checks. I performed pilot wire & transfer trip checks for years. I hated it when they went to being done by automation.
Thanks for brining back old memorys.
That was an exciting day! Another great story. Thanks for the memories.